BR “Fell”

Well it seemed like a good idea at the time....

There is a pub in Derby that I frequent called "The Alexandria" it is an old railwayman’s pub and at the back of the snug there is a picture of this locomotive -in all it's ugliness.

BR Fell ver 1.0

Very few people who drink there will have noticed its uniqueness -they will simply see an old diesel locomotive. But the Fell Locomotive was unique in that it had mechanical transmission and was designed to be a mainline express locomotive. It also had six motors, two of which were specifically dedicated to driving the “Rootes” style superchargers for the other four. This made it very noisy... But if you speak to a locomotive lover the one thing that sticks in peoples minds is, "that damned gearbox".

The Fell had the capacity to start on one motor and then add more, by clutching in, anywhere up to full power, all four motors. So, in theory if the Fell lost one or more of its motors, (which was fairly common in early BR diesels), it could still "make it home" on the others. What follows below is AN EXTREMELY SIMPLIFIED drawing of the Fell gearbox...

viz:

Fell Gearbox


In the drawing above you can see the four motors and the four output shafts to the wheels and the coupling conrods and flycranks. In the centre you have the three differentials that "balance" the power load to the output shafts. Each motor is coupled to an output shaft via bevel gears. I have not included the four fluid couplers, (one per engine), for ease of drawing and visual simplicity...

The driver starts Motor A, this transmits power to it's output shaft and some via the upper differential to the B motor output shaft, thence to the gear coupled central differential and (finally) via the lower differential to the rear output shafts... Power is thus transmitted to the eight wheels and the whole lot moves forward. As each motor is "clutched in" more power is transferred through the differentials. The net result is that all eight wheels receive the same amount of power no matter how many engines are running and at whatever throttle or supercharge pressure.

The gearbox is preserved at The National Railway Museum in York -the rest of the loco was scrapped after it caught fire at Manchester Station. There are voiced opinions that the fire that destroyed the Fell was aided and abetted by the torque convertor fluid.

What destroyed the gear box was -an ingested loose screw...

When it was built, it was a 2-D-2 configuration, with conrods connecting all four driving wheels on each side. Later on the central conrod was removed and it looked like 2-B-B-2. It is this later version that I will probably build. This will allow me to cheat and pivot each twin sets of axles, so it will in actuality be a 2-B-B-2 rather than a 2-D-2. This will allow me to get the loco around the tighter curves that my layout demands, but most important of all -it will look stranger!!!




The reason for the change has to do with the high speed rotary resonance of the huge mass of steel conrods. By breaking up their length and moving the conrods to opposing sides, they lightened the mass, and more importantly, moved the resonant frequency -to a speed far higher than the locomotive was capable of.

My quest for authenticity means that it is going to have to have four motors and three differentials. I have some ideas on how to build scale torque convertors -but I have to admit the only ones I am familiar with have Borg Warner stamped on their side... It should be possible to construct a high viscosity vane and impeller system, but what exactly the working "thixotropic fluid" would have to be is at the moment, a mystery. Olive oil and beeswax dissolved in it is an obvious one -but it is somewhat of a fire hazard...

A few weeks have passed and I have been quietly researching. I have now come to the conclusion that this loco may be actually possible to build in Internal Combustion i.e. LIVE DIESEL. This will require the building of a liquid cooling system to cool the motors. AT LAST here is something that I can put all my years of work into -and be absolutely sure that it will work!!! There are several model marine diesel engines on the market however the ones that are suitable are down to three -fortunately they are all by the same manufacturer.



I have been thinking about the problem of the torque converter... The main problem relates to the formula that I have to use, this produces a result based on the thickness of the fluid N, the cube of the input shaft speed R -and the Fifth power of the diameter of the turbine D.

This means that for a thicker fluid I can build a smaller T/C, but the more limited the speed range that it will work through. The faster I turn the shaft the more efficient the T/C becomes. The wider I make the T/C the more torque that I can push through it.

HOWEVER....

As the physicist Joule discovered on his honeymoon, by measuring the temperature at the top and bottom of a waterfall, the motion creates HEAT and it is this heat that will be my enemy if I am not too careful. What I have to do is work out the widest diameter that I can fit within my loading gauge and then how to cool it. I am looking very carefully at the original "Voith" type of torque converter as it is pumped its fluids around inside a coolant water jacket.

The T/C will have to "fall out" of connection at idle and starting speeds of the motor. Once I am happy that I have the correct motor then, (and only then), can I begin to feed the figures into this formula. The "pumping losses" that are due to the "stall" and "fall out" speeds of rotation of a T/C are translated directly into heat -and these are the ones I will have to watch out for. I have found some interesting notes on an old type of automotive fluid coupler cum clutch, (which I had seen as a teenager in the South Kensington Science Museum) -The Smith Magnetic Clutch. In this the "fluid" was a suspension of iron particles in oil and it was "thickened" by the application of a electromagnetic field. this would have the great advantage that the "N" part of the equation I could vary to fit the requirements -with a rheostat!



How it works are the field windings magnetise the rotors on the output and input shafts and then the particles of iron filings then clump to it. The gap is rapidly bridged and the whole lot rotates as one. When the field winding are turned off, the clumps are then dispersed, and the input shaft centrifuges the iron particles back into suspension. I have asked the UK suppliers of my prospective locomotive engine to send me the details, It is actually a "Glow" engine rather than a true Diesel -but it should be quite acceptable!!!

Having sorted out the prospective motor -it being a two stroke then it should be fairly easy to design a tuned output exhaust system and the equivalent inlet system. However I am not at all sure how the universal gas dynamics equation will work for so small a system... What is also provides is the possibility of actually supercharging the engine, (but in a much more modest way!!!) This could be done via a ducted fan, (such as the ones used in electric model aeroplanes), pressurising the engine compartment. I doubt that I could get much above 20mm to 30mm of water pressure but that would be enough for "proof of concept" -in that it would be operating from a supercharged environment.

Well I now have the details for the Enya SS50 marine engine and I am quite surprised at how compact and powerful it is. The idling speed is a trifle higher than I would like at 2,500 RPM but given this simple figure I can now start feeding numbers into the equations. I won't bore you with the maths but the design brief is this!

Fall out Speed of the torque convertor is below 3,000 RPM (i.e it no longer functions) -this gives me a little lee way. If I make the fluid a known one (such as 30 SAE) then I can play with a fixed point on the equation/graph. The top speed of the motor is 16,500 RPM and I doubt that I would ever go that high so let us "Top Out" at 10,000. Ones and Zeros make the maths so much easier! This gives me a working range of 7,000 RPM. To sit my tuned exhaust and inlet system within this "Power Band" -is basic maths. I would like a fairly quiet engine so it might get the expansion chamber and resonator chamber treatment...

OK -here is the std "cheat sheet" for a tuned exhaust system for a two stroke engine. I wish I could say that I worked out all of the values -but this diagram has existed since the early 20th Century...



The first question is; "Just what is LAMBDA"? Well Lambda is the symbol used for the wave length. Thus if I want the system to operate best at a wavelength of 10cm or 3,300RPM the length of the inlet pipe would be 10cm. But that is too close to the stall speed of the T/C and I really want it to operate better at the higher revs. The peak power I have decided will be at 8,000RPM (or 5,000RPM above stall speed for the T/C).

This gives the value of Lambda to be 4cm.

Well I will admit I have been busy with other things and now at the end of the Financial Year -I can return to playing with ideas!!! The main problem with this loco has been that fact that the motor will be moving at thousands of revs while at idle and several more while at power. If this was a "nitro racer" then this would not really be a problem -however my loco has to start and stop very gently this means that it will require gearing down. Not I hasten to add by the gearbox of the original -but by a far more simpler 3 stage reduction.

The "theory" goes like this...

I feed the output from the Motor through my homemade magnetic clutch system and by varying the field strength I can have from 0 to 100% transmission. The output shaft then feeds the first stage reduction gear, this then feeds the second stage reduction gear located centrally between the two power bogies. The output from this feeds a central shaft to two Universal Joints located directly at the pivot points of the bogies. Then from here it feeds a worm and spur gear to the OUTER axles of the power bogies. The INNER axles are then fed power via the external fly cranks -in the exact reverse of the original manner!!!

See Picture 6.


The "maths" runs something like this

The First Stage reduction is 1:10

The Second Stage reduction is 1:10

The Worm and Spur Gear is 1:30

Therefore the TOTAL reduction is 10 x 10 x 30 = 3,000 : 1

This may seem to be pretty excessive -but remember that the stall point of the torque convertor will be 3,000 RPM.

Now, if we assume that we are running at 100% transmission and the driving wheel diameter is 5cm then the revolutions of the wheels will be 3,000 RPM.

The speed the loco will be travelling at will be 3,000 x Pi x 5cm per minute = 47,130 cm per minute. This rather alarming figure drops down to 7.8 metres per second, still rather on the high side, but this is a perfect case scenario!!! At best I think my clutch will be 10% effective -this gives a far more respectable 78cm per second. This equates to a "rough" 20MPH at scale speeds.

Well -slowly but surely things and ideas are starting to come together... Over the past few nights scribbled bits of paper with dozens of rubber marks have come together to produce the following "chassis mk1" drawing.

See Picture 7.


Everything can be welded together from 3mm plate stock(!)

I know that a few months have passed since I last made an entry onto this thread -but I have been busy -with home and work. I have decided to use the ENYA SS/50 Marine engine for my power plant. This is "slightly" overkill for a Gauge '3' model -but it is a very common IC engine and parts are easy to obtain. Experiments with the magnetic clutch system were errrmmm... "Interesting" as the amount of fluid and iron filings that were sprayed when the sides of the containment vessel breached were spectacular!!! I never even thought about the amount of force that the spinning oil and iron filings would exert on the sides of the clutch. I have come to a 3 plate clutch of the "wet plate" variety operating in a fillable oil bath. This closely resembles the "MekHydro" torque system, no I didn't crib the idea! But the problem is how to pump the oil that provides the frictive medium in and out of the clutch vessel.



I have found a source of wheels for this loco that are an exact match -but where they are from is probably correct too... The Driving Wheels are an exact fit for an LMS "Duchess" and the Bogie Wheels are an exact match for a tender for a "Duchess". I am not saying that BREL Derby had a few hanging around -but it does fit the ethos and manner of the Litchurch Lane Works!!!

The final part of the assembly drawings is now complete. I know how to make it reverse... This may not seem a major achievement but the reversing mechanism is one that has bothered me for some time. So, in my typical manner I decided to cheat. I have a design for a reversing mechanism that goes forwards or backwards whether it is going round -or not!!! I have decided to adapt the standard method of dog bevels. These do not transmit very much torque -but the system should only be going in reverse for short periods... The drawing below shows the arrangement for it.

See Picture 10.

Models are getting completed thus other models rise up the construction ranks. This is what is happening with this model. I have the majority of the parts figured out and some of the prices. This is of course highly elastic as there have been occasions when I have worked out parts and suppliers only to find that, not only are the parts no longer made -but the supplier is now defunct!!! As this is a diesel model and will operate at a fairly high temperatures the bodywork is going to have to be made from metal. This is a radical departure for me as readers will know wood and plastic are more my medium. The body is going to have to made from Aluminium sheet. This is because it is light and very ductile. I have a small “fabricator” which consists of a Guillotine, Folding Break and Rolling Slips built into the one chassis. Whoever coined the sales term “light weight and portable” obviously never had to lift and shift this brute. I am not the puniest of people, but humping 45Kg around my small work shop is very bad for my back... Most of the time the fabricator lives on the floor on a slide out shelf, (I wonder why???), but for some jobs it has to sit on the top of the work bench.

Most of the body work is simple curves that can be rolled in the slips and there are some compound curves where the corners meet. But that is wooden dolly and sand bag work and can be formed by hand (hitting it slowly) with a “Repousement” hammer and a “Cloth and Hide” mallet. Joining the sheet metal sections is going to be “fun”. The normal tricks of soldering , brazing , and welding are not going to work with Aluminium. What I am going to have to learn is the magical art of “Aluminium Welding”. I put the brackets around the last part as my best friend refuses to call it welding -he is an instructor at “The Welding Institute” and he prefers the term “Eutectic Solvent Union”... Despite this I am going to use the words “Aluminium Welding” as, (to me), this is easier!!!

I will use non fluxed rods -in short the “Techno Weld Process” to create my shell that I will simply lift off and drop over the loco.
September -the start of the new school year and the start of this locomotive. Today is my son’s 11th birthday so the first order for the parts has gone out to the steel stock holders.

Bogies:
3mm                          bright mild steel flat

20mm x 50mm          2 rqd
20mm x 87.5mm       2 rqd
30mm x 115mm        4 rqd

Traction Chassis:

3mm                          bright mild steel flat

40mm x 300mm        1 rqd
50mm x 90mm          2 rqd
50mm x 30mm            2 rqd
50mm x 130mm        4 rqd

Power Chassis:

5/8th" x 5/8th" x 16SWG wall

500mm                      2 rqd
120mm                      4 rqd

After the accountancy job with the “Krokodil” I am loathe to do it again -because this is going to be the most expensive locomotive I have built so far.... But on the other hand perhaps it would make a good contrast to show what can be done on a restricted budget of £10 per week.

Ok -so what has changed in the intervening months since the design phase was “completed”?

Well, I have found that the manufacturers called “ASP and “Super Custom” make a more suitable range of Marine engines for model locos than “Enya”. These range in size from 0.12 cu in to 0.91 cu in. All the calculations are for the Enya SS/50 engine -but the price comparison between the manufacturers is “interesting” (!)

The 0.91 cu  in motor is very tempting as a power supply as it has the flattest torque curve and slowest idle of the group.

All the fluid calculations were also based on SAE 30 automotive motor oil -which is for some reason is suddenly becoming very hard to find(?) The reason I chose this was its characteristics at all temperatures are well documented and there are no “additives” that change the viscosity with temperature as in a modern motor oil. Thus the viscosity at any temperature, pressure and rotation can be read off the graph. The alternative is to use good old fashioned Castor Oil as a medium for the torque convertor -but this will undergo oxidation in quite a short time interval... The other thing to consider is that the oil will be returned from the torque convertor looking like, and with the consistency of: dirty “whipped cream”. The pump will force cooled oil into the convertor and a large bore pipe will return the oil to the tank where it will separate and hopefully it will disperse back into oil and air. One of the things I am going to have to look out for is the danger of my model “exploding” in a sea of oily froth.

If I go for the 0.91cu in motor, (as now seems likely), then the cooling system will have to be adjusted to suit. The size of the radiator is going to be doubled -to two rows and there will be “tinselling” on the vanes to improve air to copper mixing. This also means that an Ice and Water tank is now a Definite rather than a Probable. Thus the direction of coolant air in the loco has to be reversed. Instead of blowing air INTO the loco I now have to blow air OUT of the loco. Initially I was going to blow a draught of air along the length of the loco -but it seems that there are going to have to be some auxiliary fans to do this whilst the radiator fan sits in a sealed environment. The electrical supply for them is going to have to be from a NiMH bank of cells. I know that I normally use Sealed Lead Acid batteries -but on this model I don’t think that is any room for them and the environment could be a little “hot”....

There is actually a design “progression” in my models. From this locomotive I learn about using a 2 stroke glow motor as a power plant for a loco and the cooling problems inherent with it. The next loco is a diesel electric in which I learn about the problems of building an alternator and the power bogies for it. The next loco is a gas turbine electric  in which the only problems I now have to crack are those of actually making a working gas turbine since all that goes with it has been already been built!!!

As they say around here “I may be crazy -but I am not daft”

I posted what I had done to a forum, (I know call it vanity if you like -I prefer to call it explaining!), I got some useful comments about sources for SAE 30 oil. The most common source of it nowadays would seem to be garden machinery...

This is my reply.

“No, it has to be the automotive stuff because the SAE Rating of your common or garden(!) lawnmower stuff is not designed to operate at 0 deg C. If you examine the drawing above you will see that the oil feed to the torque convertor passes through the Ice and Water tank. By fixing my oil temperature at 0 deg C I can then accurately know what the viscosity of it is.

So, what I want is a thick treacly oil that will get thinner and easier to flush out when it is hot and not foam too much. I know that SAE 30 is usable from -10 deg C to 100 deg C and the viscosity varies from 9.3 to 12.5 Centi-Stokes (mm sq per second) at 100 deg C.

Strangely enough if you examine the sizes and viscosities of the design above -there are lot of 0s and 1s on both sides of the equations.

I am an inherently lazy mathematician... “

Silkolene in Belper is where I used to get most of the SAE 30 from -but they have stopped making it!!! The only real source is Comma, who sell it for £14 per gallon -however there does only appear to be two tins left in the entire UK???  "Gertrude" runs on MOTIL 1 -which is a great oil -but totally useless for this as it retains the same viscosity whatever the temperature...

It is not the lubrication aspect that is important here -it is the viscosity at 0 deg C.

My home made gear pump is going to be made from Hostaform using MOD 2 gears so that rules out any form of thixotropic wax, (i.e. Automatic Transmission Fluid).

"Rob" has given me a quote for the start of the steel. This has been duly paid for via "plastic" and I await delivery. I now have to design my bodywork... The body is, in theory, two cubes stuck onto the ends of a rectangle with an arch over it. But as anyone with even a little knowledge of stereo geometry will tell you "HA HA -no it it's not"...

So it looks like I will have to fight my wife for possession of the left over cornflake boxes to make "pattens" from. She normally uses them for Quilt Templates.

I have been researching my wheels over the weekend and come to the conclusion that the "perfect wheels" are too damned expensive. These are the tender and bogie wheels for an LMS Duchess -however if I accept that they are 1 spoke too few then the wheels from 4 foot and 3 foot wheel castings from Walsall Model are a better bet. Having no experience of machining cast iron I would rather "crack" a cheapish wheel of £4 than one of £30. I think in this case it is an example of "all the traffic will bear"...

The problem is that you CANNOT trust the original calculations as provided in the original -because very few of us have gardens capable of 6 chain and 8 chain (scale) curves. This means that you MUST recalculate all the parameters for your model before you begin construction.

If you take the dimensions as provided by BR you end up with this...

See Picture 11.

This CAN be made to work however quite a bit of cheating will be required to get it around my std 2.2m radius curves. If you examine the "nice" drawing above all the distances are regular and the manner of its entry and exit to a curve are predictable as it is all a segment of a polygon. What now has to be done is to "ditch" the Bissell Bogie at either end and replace it with an Adams Bogie on a control arm. The will enable the Adams Bogie to rotate far more than a simple spring system would alone, and also to traverse more easily. The result is that the Adams Bogie does not steer the Loco as much. However if the Adams Bogie is spring coupled not to the Power Chassis (red) but to the outer part of the central bogie of the Traction Chassis this force will act on it to steer the bogie (or more correctly pre-load it) as it enters and leaves the corner. The Adams bogie is also going to have to have independent turning wheels i.e. the wheels will have to be able to turn on bearing fixed on the axles not the axles themselves...

This will stop the flanges trying to "climb the rails" due to the forces that would be transmitted through a connecting axle.

At the moment I am having "fun and games" designing the one thing that I will admit that I am totally useless at, (other than welding!), and that is gearbox design... I have something on my drafting board that fulfils all the criteria -except beauty. On the other hand this locomotive is infamous for its gearbox -so I should take some heart in the matter. Whether the locomotive will performs with "seamless acceleration" as the original was supposed to do, (or as it was claimed), but just in case I will keep close track of all screws locally!!!

I have a “number” of old DP sintered iron spur gears wheels -these are basically metal powder pressed into a mould and heated until it all fuses together. I think I have had them for over 15 years now -so it is time for them to pay me a little rent money... They seem to be the curious ratio of 38:16 (yes I have counted them twice to be sure!) One of them will form the output gear of the torque convertor and this will drive a cascade of three of them giving an output of 1:13 (!) this then feeds a 12 tooth 0.7 MOD gear to a 100 tooth 0.7 MOD gear that drives the reversing dog bevels. The output shaft from this then drives a second set of bevels to a worm and spur gear set up of 1:50.

So, at the end of this

1:13 from the torque convertor
12:100 from the reversing dog bevels
1:50 from the worm and spur gear

Which is the wild figure of 1:5,146.66 recurring...

Most of this is going to have to be transmitted through Iron and Hostaform gears using 6mm shafts. These are going to have to be mild steel or possibly brass. This is because the real alternative is “Silver Steel”. Which would be marvellous -if I could actually get a drill bit through it without it wandering all over the place.

This locomotive relies on one thing -that the torque convertor works!!! Having worked out; how the oil will interact with the discs, the sizes of the holes in them, the expected heat transfer due to friction and finally the force of the oil on the sidewalls of the container(!)

The one problem that is still problematic is, how to put the damned thing together...

The only way I think to do it is via the "Layer Cake" method. I make some plywood discs and assemble first the impeller disc, a sheet of plywood, a driven plate etc etc. The central shaft is then silver soldered to the impeller disc and the next layer added. Eventually after three iterations I have a stack of discs, burnt plywood and plates. The position of the holes in the discs does matter. The impeller discs are aligned so that the four holes will overlap producing a spiral. The driven plates are aligned so that their holes produce a spiral in the reverse direction. This means that the impeller discs force the oil right to left and the driven plates accept the thrust generated from it.

The driven plates have to be larger than the impeller discs -so that the torque from them is larger than that supplied by the impeller discs. The oil viscosity is measured in mm sq per second. This makes the maths simple, the torque increase is the area of the driven plate divided by the area of the impeller disc -provided we ignore the changes in the viscosity of the oil due to the rise in temperature due to friction!

This gives me (see above) 8 faces of driven plates to 6 faces of impeller discs, which works out to 8 x  (2.54 cm sq) divided by 6 x (1.27 cm sq) which equates to 16 / 6  = 2.66 recurring.

The interior of the torque convertor chamber is going to have to be profiled to provide a profiled smooth “return” to the moving fluid -this will be done on a rotary table and a ball ended mill. The oil is going to have to enter the torque convertor at the base of it and exit at the centre. This may seem strange but remember that the fluid will be moving with the driven plates and centrifugal actions will force it to the walls. Thus the centre of the torque convertor IS the top!!!

The pump will have to empty and then fill the torque convertor chamber for starting the IC engine and changing direction -thus the pumps default mode of operation will be to EMPTY the torque convertor chamber. Allied to this there will have to be some form of “parking pawl” on the torque convertor output gear to lock all the gearbox and transmission static once it has done so, and to release once the torque convertor chamber starts to fill...

How I am going to do this I am in two minds about. One option is to use the level of oil in the chamber to block an IR LED -the other is simply float something in the oil tank and close a switch with it! The tank volume is going to be 500 cm3 (for ease of maths!)

The pump controls the level of oil in the torque convertor and since it is, (hopefully), at 273.16K the viscosity has to be 12.3 mm sq per second. The volume of oil pumped into the torque convertor has to be Pi x R x R x H which comes out to 3.142 x 3.5 x 3.5 x 3 = 115.5 cm3. If we assume a fill time of 3 seconds this means that the pump must be capable of roughly 40 cm3 per second or 2.5 litres per minute. This is also the rate of flow of oil through the Water and Ice intercooler... The question I now have to ask is how fast do I have to turn my pump gears? Since I am going to use MOD 2 gears they have pretty coarse teeth. The smallest gear I think that I can get away with is a 12 tooth. This works out at a diameter of 2.8cm and a tooth depth of 0.2cm. This means with two gears I have an effective driven volume of (Pi R sq H) -(Pi r sq H) per revolution, (the teeth occupy 50% of the volume of a gear wheel).

So:   Volume    = [(3.142 x 2.8 x 2.8 x 1.5) - (3.142 x 2.4 x 2.4 x 1.5)] per revolution

                        =  33 - 27

                        = 6 cm3 per revolution

Thus my pump must turn at at least 420 RPM to fill the chamber in the allotted time. Now to work out how much torque the pump motor has to deliver. This is (thankfully) simple mechanics.
The torque required is that to lift 6 cm3 of oil with an SG of 0.8 a distance of 2.8 cm with an arm of 1.4cm

Torque = (6 x 0.8 x 2.8 x 1.4 ) = 19 Gramme Centimetres

There are several motors of this rating available -but what we need is one capable of generating this torque at the, (fairly low), revs of 420 RPM. This will mean searching for a motor with a wide but short armature -ideally one that is roughly the same diameter as the gear wheel. This will mean driving the pump motor from a PWM supply as this will deliver full torque at all speeds -again the pulse frequency will have to be low to encourage high torque in this situation. The MFA RE-360 is probably overkill -but it will just keep going!!!

The heating effect of friction is the rate of rotation and the area of the discs divided by the viscosity of the fluid. The Specific Heat Capacity of the oil “should” be 2 Kilo Joules per Kilo Gramme per deg Kelvin. So the mass of my 500 cm3 tank of oil is 0.8 x 500 = 400 Grammes. This means that the amount of heat that has to be used to raise it’s temperature is 800 Joules per deg Kelvin.

Unlike Joule I had other things to do on my honeymoon than measure the temperature at the top and bottom of water falls!!!

The manufacturers spec says that the IC engine develops 2.2 Kilo Watts, (or more usefully here), 2,200 Joules per Second. So, if my torque convertor is ZERO percent efficient then the oil temperature would raise by [ ( 500 / 115.5) x (2,200 / 800) ] = 11.9 deg K per second!!!

So, what is the safe level of efficiency?

I am going to assume that my torque convertor is 75% efficient -or rather that I have to dump 25% of the shaft power as waste heat into the Water and Ice intercooler.

Ploughing through the maths gives an output temperature of 276.13K and the oil now has a viscosity of 11.73mm sq per second. This gives me the amount of heat I have to "dump" through the intercooler and the expected life of the ice in it. If I construct a tank holding 1,000 grammes of Water with 1,000 grammes of Ice then the entire volume of oil (400 grammes @ 276.13K) gets cycled roughly every 12 seconds.

This gives me a thermal input of 5 x (2000 / 400) x 2.97 Joules = 75 Joules per second.

To melt 1,000 grammes of Ice to Water takes 334,000 Joules = (334,000 / 75) seconds of running time or 4,453 seconds or 74 minutes (roughly).

The exact Specific Heat Capacity of the SAE 30 oil I will get is as yet unknown. I think I will have to do the ‘O’ level Physics experiment of boiling brass kitchen weights in water and dropping them into measured volumes of oil, measuring the temperature rise, and then calculating it from that.

Despite all this the one major source of heat is, the IC engine that drives this loco...

Having decided on an Ice  and Water cooled system -why do I need a radiator for the IC engine? And the answer is that MOST of the time -I won’t... However when the IC engine is really “clogging it” then the temperature of the returned water will be higher than ambient and it will need cooling. Thus the fan speed with depend on the temperature of the returned water. This will be a simple thermistor located in the return feed to the radiator feeding it to a PWM driving the fan. I am a purest but not even I am going to produce a “wax stat” for the radiator! The pump motor will be the same as that of the torque convertor, (I think it might be wise to make three in total)...

OK, so what are the cooling requirements for the IC engine?

Oddly enough -not that high... UNLIKE the torque convertor this is an “open” system. The high temperature component comes from the exhaust, which is dumped to atmosphere, so all that is required is enough cooling to keep the cylinder head (and glow plug) within parameters. The water feed intake will be at 273.16K and the outlet temperature at higher than 280K before the fan triggers. The Specific Heat Capacity is slightly over twice that for the oil -so it gets hot slower -but it also gets colder slower too. I can dump most of the heat via the radiator before it returns to melt the ice. The curious thing is that I might be in the position of having to cut down flow through the radiator to stop the ice cold melt water warming up from the ambient air in high summer. One possible way out of this is “sacrificial cooling” in which I squirt some of the ice water onto the radiator, and the evaporation of it assists in the cooling of the water. A similar thing was done on the Reed Ramsey Turbine Electric. The limiting factor for this is of course that you will run out of water to cool and pump around at the same time...

The only way out of this is a method I don’t like.

I am going to have to link two independent PWM supplies to the same thermistors in the water circuit from the outlet side of the IC engine. This will have to control the PWM supply to BOTH the water pump and the radiator fan. What I am afraid will happen is “short term ripple”. The system begins to range between too fast and too slow -it can get into a type of positive feedback. I think that the trick is going to be to attach the thermistor to a “damping block” of metal that will heat and cool a lot slower than the water around it. I then take the output of the thermistor and tune the two PWM supplies (pump and fan) to match it.

This is my pump design. It uses two  MOD 2 Hostaform gears from Muffet Gears (part number S2.0 012H). They have an 8mm bore -which is unfortunate! This means that I will have to fabricate an adaptor to the 2.3mm shaft of the RE-360 motor. The easiest way to do this is probably to just to connect the driven shaft of the pump to the motor via gears. A push on MOD 1 gear to the motor and a bored out to 8mm MOD 1 gear to the shaft. There is plenty of “meat” on the boss of the MOD 2 gear to directly pin the MOD 1 gear to it with four M2 nuts and bolts...

See Picture 12.


Below is my “standard” PWM circuit -but in this case(!) I have replaced the 100K log potentiometer with a pair of 47K thermistors. These are NTC (negative thermal coefficient) i.e. the warmer they become the more that they conduct. What can happen, (and I am ashamed to admit It has happened to me), is that the current running through the thermistor actually heats it up!!! The water passing over the thermistor should dump the heat from it and (hopefully) simply allow the thermistor to work.

See Picture 13.

So, (in theory), this is what happens! The IC engine coolant return water gets hot, this lowers the resistance of the two thermistors which increases the pulse length in the PWM. The motors pick up speed and then more water is pumped across the cylinder head, cooling it down. This lowers the temperature of the coolant return water and increases the resistance thus the pump and fan slow down. The dangers of “short term ripple” will mean that I will have to fiddle with the thermal mass (the metal dampening block that the thermistors are bolted to) and fine tune each PWM with a set of multi turn potentiometers.

Having nailed down the cooling of the cylinder head and the cooling of the torque convertor the one great question remains -the radiator. Fortunately I am something of a “petrol head” and I am a “computer geek” as well. Both of these have now glorious united in this design problem... My solution is one I have used before and long before it became “trendy” I was using liquid cooled computers. Modern methods are to cool the CPU directly and dump the heat outside to a fan driven radiator via brightly coloured coolant fluids. My solution is ugly -although it will have green food colouring in the coolant to aid topping up(!) The temperature of the output from a 91 series Marine IC engine cylinder head has been measured, (Thank You “Lady in Blue”!), the flow put through it however was not possible to measure as it was fed from a scoop that the boat pushed  through the water. However I do have an input temperature (12C = 285.16K) and an outlet temperature  (26C = 299.16k).

The fuel used was a 15% Nitro Methane, 20% Castor Oil,  65% Methanol blend set to “rich” with a “cold” glow plug. This is going to be more thermodynamically powerful than the stuff I intend to burn which is a simple 20% Castor Oil to 80% Methanol. So, if I take the temperature differential as being 14 degrees I can plug away at the maths...

Ok -lets assume that the pump normally operates at the same rate as the torque convertor pump i.e. 6 cm3 per rev. The coolant enters the cylinder head at 273.16K and leaves the cylinder head at 287.16K this means that the radiator design has to dump 6 cm3 x 14 degrees = 84 Joules per revolution. But it gets worse... The pump rotates at 420 RPM this means that the throughput is 6 x 14 x 420 = 35,280 Joules per minute or more usefully here 588 Watts - yes about the same as a small domestic fan heater...

The main problem is that, despite what it might feel like, temperatures of 0C or 273.16K and below in the UK climate are actually fairly infrequent(!) The normal ambient temperature for easy running is probably between 10C or 283.16K and 20C or 303.16K. This means that the lowest temperature that I can cool my return coolant to is from 303.16 to 283.16K. By simple equation the amount of dry air that I need to pass through my radiator to do this is 20 Litres per Second.

From an engineering perspective, a radiator varies from an ideal black body by a factor, ε, called the emissivity, which is a spectrum-dependent property of any material. Commonly, a fluid thermal mass, containing the heat to be rejected, is pumped from the heat source to the radiator, where it conducts to the surface and radiates into the surrounding cooler medium. The rate of heat flow depends on the fluid properties, flow rate, conductance to the surface, and the surface area of the radiator. Watts per square metre are the SI units used for radiant emittance. If the system is not limited by the heat capacity of the fluid, or the thermal conductivity to the surface, then emittance, M is found by a fourth-power relation to the absolute temperature at the surface. The Stefan-Boltzmann constant is used to calculate it, as M = εσT4. Since heat may be absorbed as well as emitted, a radiator's ability to reject heat will depend on the difference in temperature between the surface and the surrounding environment. For particular operating temperatures, a system's overall heat flow may be given in thermal watts, abbreviated Wt.

I have been working out my radiator... Classically there is only one metal to use -and that is Copper. However Copper is increasingly expensive and has no real alternatives, other than Gold or Silver -for conductivity. There are two major designs for a radiator, the one most modellers are familiar with is the “square spiral”. This is simple to produce and works well. It is a length of pipe soft soldered to a strip of metal and the whole lot wound in a spiral like shape. The “automotive” multiple tube type is the one that I am going for. This is because it will be the most difficult to produce and hopefully once it is complete other people will see how to produce one for themselves. The material I am going to use to build it is BRASS... I can hear the screams of “De Zincification!” from here. However since most of the time the radiator is going to be empty the Zinc problem will  not be that bad, (hopefully). Added to this I will be using distilled water and ice made from distilled water this means that the ion exchange that leeches the Zinc out of the brass should be slowed down. But if the plumbing does spring a leak then I have only myself to blame for it!

The top and bottom tanks will be made from Brass “L” section soldered together to produce a square section tube -the ends will then be plugged in the normal manner with a piece of Brass sheet (this also gives me the mounting holes...) The tubes will be made of 3.2mm 24SWG brass tube and they will have their ends cut at 45 degrees to ensure that if the do slip whilst I am soldering them into position water will still get through them. There will be 60 tubes each effectively 8cm long giving me a surface area of 482.5 sq cm. This should work as a bottom feed system, i.e. the radiator fills from the bottom upwards -thus flushing out any air in it. The cooled water then returns to the top of the tank and moves the ice around ensuring good thermal mixing!

See Picture 14.

Well having paralysed everyone with the raw maths perhaps I should break it down into simpler chunks?

The bore of each tube is 0.3 cm making the cross sectional area 0.706 cm2.

The pumps supplies coolant at 2,500 cm3 per minute across the radiator.

Each of the 60 tubes passes coolant at the rate of 0.7 cm3 per second.

The fan passes 333 cm3 of dry air over each tube per second.

Thus each pipe has to pass 9.8 Joules of heat from the coolant to the air in 1 second.

This gives a radiator rating of 9.8 Joules per 0.566 cm3 per second or in SI 17,647 Watts per sq metre.

So, as further proof of my lazy mathematics -hands up those who noticed why the radiator design has SIXTY tubes....

Having worked out some of the “mechanicals” I now have to work out the bodywork. This is as I have said going to be made from Aluminium sheet with the sections welded together. This will involve some work with a sand bag and a “Repousement hammer” and I foresee quite a few “words” as the metal refuses to go in the right direction... The thickest metal that I can cut and roll with my “lightweight fabricator” is 0.1cm thick and 30 cm wide. I do have a 0.1cm “joggle” set for my joggle pliers. These are strangely named things which simply produce a stepped edge when the two jaws are brought together. The plan is that I cut strips and then roll them in the slips part of it to the correct curvature and “joggle” the edges to get the overlaps for welding. This will leave me with a section seam that (hopefully) I can fill and polish smooth. The formers that I am going to have to make to “bash” the metal to shape over I will make from plywood. That and handy lengths of steel bar and a lump hammer hitting a sand bag over the two will produce the correct high curvature that is required for some of the parts. I admit when I first saw this technique I was horrified!  But the sand transfers the impact evenly and forces the metal to move across the former.

The bonnets at the ends of the loco are going to cause some “fun and games” as well. The ends are square these then rise to form a curve at the windscreen... So, rather than forming section through a frustum, (which would be so easy!!!), they instead will have to be radially step folded and the folds bashed smooth(ish). The rest of the bodywork is (thankfully) not so wild -but it does have some tight curves at the corners that will have to given the sand bag and lump hammer treatment.

See Picture 15.

The next step is to “crack” the problem of the windscreens themselves... These should be three simple panes of plastic -however the shape of them in somewhat “unique”.  The curve of the roof is a a pure arc of 7cm radius and the top of the bonnet forms a pure arc of 13.2cm. So far so good. The problem begins as the windscreen is inclined at an angle that is not a “normal one”... The angle is 1:2 or horribly enough 26 degrees 43 minutes from the vertical. I will not ask why they did not make it 30 degrees -as this would have been too easy!!!

Flipping through the Sine,Tangent and Log tables section of “Zeus”... The central windscreen presents a frontal dimension of 4cm x 2cm whilst the vertical dimension now works out to be 2.2cm and the base of the side windows work out to be 1.3cm.

If you consult the drawing above you will be able to see the rough position of the panels. The longest thing that I can roll is 30cm  -thus the roof is rolled as one complete section and then the flanges “joggled” to it. This is going to have to be a monocoque structure and I am not quite sure if I simply design it to lift off as a whole -or to have a roof access hatch. The former is going to be the stronger whilst the latter is probably going to be the easiest to operate with(?) This is not a simple question. Starting a 0.91 series Marine motor is not something that can be done with a flipped finger on a aero propellor. Smaller engines have “pull starters” whilst the larger ones have external battery electric starters operated via captive rubber belt. One of the “radiators” on the nose is probably going to have to be an access panel for the captive rubber belt. This will not be a problem with the diesel electric locomotive as the starter motor is the generator.

I could laugh! The motor dimensions are all metric -except the screw thread coupling from the flywheel which is a 5/16ths UNF thread... I of course, have no UNF taps.

According to the e-mail from “Rob” the nice man should deliver my steel sometime tomorrow. I am starting to “itch” quite badly!!! As promised the nice man did turn up on the doorstep at just before 10:00am. and I duly unwrapped the very well wrapped pieces of steel. Here you can see them on the side of the cooker -yes next to the kitchen sink....

See Picture 16.

A quick ID Parade is as follows.
On the far right there is the length of the chassis plate and the longitudinal sq tube for the power chassis.
On the top left there are the B plates for the power chassis and their top spacer plate.
Below them are the 4 transverse sq section tube that for the rungs of the power chassis.
On their left are the bogie spacer plates.
And finally on the bottom are the side plates, arms for the front and rear bogies and the bottom spacer plates for the B plates.

Having looked at the drawings above you might think that I have cheated (which is normal for me!) and I have two central pivoting bogies. But technically this is not true... What I have used in this loco can be classed as a Beugnoit lever system. The Beugnoit lever (Beugnoit-Hebel) is a mechanical device used on a number of locomotives to improve curve running. It was named after its inventor Edouard Beugnoit. Around 1860, when Beugnoit was the chief engineer at the firm of Köchlin, he developed a system whereby wheel sets are housed in pairs in the locomotive frame, with side-play, and connected by a lever. These levers are fixed to the frame in the centre and thus enable the sideways movement of the connected axles in opposite directions. In this way, instead of being fixed in the frame, the axles are able to move sideways rather like a bogie, but clearly nowhere near as much. On locomotives with a side rod drive, the axle side-play is balanced using longer coupling pins (Kuppelzapfen) on which the coupling rods are also able to move sideways.

On running round a bend, the first axle is pushed sideways by the curve of the rails and so moves the second axle parallel to it in the opposite direction, until the wheel flanges of both axles align with the rails. This distributes the guide forces between the two axles which reduces wear and tear on the wheel flanges. By enabling this transverse movement of the wheel sets, locomotives with rigid frames do not have to use the thinner wheel flanges etc. normally needed to facilitate smooth running through points, bends and tightly curved sections of track. The 'guide length' of the locomotive is formed by the distance between the two fixed Beugnoit lever pivot points.

See Picture 17.

 In Germany, Beugnoit levers were used mainly in the middle of the 20th century. The best known examples of locomotives that use this type of lever are the MaK side-rod drive locomotives, the Class 105 and 106 engines in East Germany (DDR) as well as steam locomotives like the DB Class 82.

Since this locomotive is “steam era” design technology then it does rather make sense to use this. The “Adams style” bogies are another “steam era” device that I am using. These will “pre-load” the chassis when cornering, whilst putting them on a floating arm will enable me to control them in a more predictable manner.

I am now in the first stages of turning my “primitives” into the shapes that they will be on the finished loco. The first things to do are to produce the Bogie side plates. This is a simple process of chain drilling and (ugh!) lots of grinding and filing to produce the half dog bone shape that they require. It may not be prototypically correct -but I have opted for a simple 1cm radius from the centre of the axle for my dog bone curve. The Bogie wheels are going to present me with a problem... The last set I made were mounted as a floating  wheel between two sets of ball races. These will have the no journals so I am going to have to do some ”brainstorming” with some friends as to how I will connect them to the axles. The favourite method at the moment is to drill out the centre of the bogie wheels and insert the bearings on an allen headed bolt into the axle -which I have bored and tapped to that thread. Once the thread lock has set solid (a short pause for the oven...) then I can grind off the end of the allen bolt to a flush end. This is all very well and good -but until I actually get the wheel castings in my fingers this is all theory. However on the plus side of the argument it does seem that it can be made to work! If it does work than this will give me a free rolling bogie with no cornering problems due to the wheels rotating at differing speeds. Ideally the coning on the wheel should give me the differing effective rates of rotation that I need. However I really am that cautious!!!

I have often said the British do business in the pub. Yesterday I went to a beer festival and supped some nice stuff (and one VILE concoction -not unlike trying to drink battery acid!!!) There amongst the books at the beer festival (held at The Great Central Railway in Loughborough) was a book to die for. It has the dire name “British Railways Design,Theory and Operation of Diesel Locomotive Traction Volume 1”. They wanted £8 for it. I did explain that I had come to the beer festival to drink beer and not really to buy books. They said I could have it for £5. I offered them £3 and they willingly took it. I placed the money in the tin, walked out of the “shop” (a converted horse box), turned the corner, and then ran like a thief!!!

It is PACKED with drawings, formulae, tables and installation instructions plus (oh thank you!) worked examples. I now can very accurately reproduce BR transmission fluid for a “Western” and DERV of a Cetane rating to run a “Deltic” with... If I am right(!) the hydrostatic formulae in the book point to me needing a smaller engine than the .91 series that I was thinking of. This means that it will be cheaper to buy, create less heat, (and thus cooling), whilst producing a higher torque from the convertor. Given the tables in the book I can now successfully “dope” my SAE 30 oil with additional additives that will give it a higher thixotropic factor than it would have simply as a cold liquid. All the substances mentioned are commonly available and I have decided to use Aniline, Canubra wax and Flax Oil in a 1% 5% and 10% mix with the SAE 30 oil. This will give a smoother transition from a “liquid” to the “solid” as the rotational speed difference between the driven plates and the impeller discs alters.

The common sources for Canubra wax are shoe polishes -but the raw stuff is available from artists and cosmetic suppliers. Flax Oil I got from my local Health Food Shoppe. The assistant then explained how it would be good for my skin and muscles and how to consume it with “normal foods”. I then explained that I wanted it for putting into the torque convertor of my model to alter the thixotropic co-efficient (Rho) whilst still maintaining the di-oilic paraphase constant (Phi) at the point of solidus (Kappa) in a Standard Temperature and Pressure environment. At which point she asked me to enter my PIN into the EPOS terminal...

Anyway -this is how it works(!)

The motor is idling at 2,000 RPM there is no fluid in the chamber. I pump fluid in and the drag begins to turn the driven plates. The fluid now fills the chamber and the drag between the impeller discs and the driven plates causes the fluid to slow down between the plates -this makes it behave more like a solid. The impeller discs and the driven plates now move at the same speed. The fluid now acts as a solid between them despite the fact that the whole thing is going around at several thousand RPM...

Only the fluid at the edges of the chamber behaves like a fluid, whilst it is between the discs and plates, it behaves like a solid.

I have begun to accurately machine the primitives to size. The first things to go into the jaws of the mill were the two longitudinal square section tubes. These need to be cut to exactly square ends -otherwise nothing will line up.... The problem I have at the moment is that there is “Dobbin” the rotorvator stashed in the workshop. It seems to take up 50% of the available area whilst only occupying 5% of the floor! Dobbin is providing muscle to produce the lawn that the railway will run around -so it has to be handy for when the weather permits him to function. The soil has to be just right for the tines to cut through the clay -otherwise he just stalls. Too wet and it just churns it to slurry... Anyway as you will gather some fun and games were had getting the mill , its vice, and the sticking out lengths of steel in a position where the operator could use it with out recourse to advanced Yoga positions. I loaded the EM32 collet with a 10mm HSS cutter and began to nibble at it. After a few passes I had a nice square edge and some tape holding everything together to flip and do the other end. The transverse pieces are going to have to wait until I have been at them with the hacksaw, as I need to produce a flap edge for the ends. When I start welding them into position I can safely weld an end plus both of the laterals. The last end will have to have a bolt arrangement as this will carry the motor and the torque convertor on it. This will make it easy to remove as a unit for working on.

ALWAYS design your models to be easy to work on!!!

After some delay caused by domestic priorities, (my son has to choose his Yr 7 school and I have been ferrying the assembled to the various “Open Evenings” at schools that are available). I can now return to building a loco. This Wednesday I plan to order my wheels from Walsall Model Industries. They are not the “correct” wheels for the loco -but they are a fraction of the price of the “correct” wheels.

The ones I am going to use are GWR ones....

The bogie wheels are going to be the 3 feet 3 inch bogie wheel part number: T1818 and can be machined between 39mm and 44mm. As the size I need is 40.5mm this is well within par. The main driving wheels will be the T1841 casting the size of this is between 49mm and 55mm and is thus a little “shy” of the required size at 57mm, but to be honest it would cause the model to sit 1mm lower, have 2 spokes less per wheel, and at a saving of £60 -I can live with it!!!

I have never worked with cast iron so this is going to be a “first” for me. All the books say to take a heavy first pass to get rid of entombed grains of casting sand and the toughened skin that forms as the shock cooling of the molten iron occurs. It is also in the books that this is going to be noisy, so I have alerted the Domestic Goddess to go out to the Summer House and quilt etc -whilst I am busy at the lathe.

Well the wheels have been ordered and then steel is starting to be machined to size. The Mill has however done its usual trick of blowing the fuse holder -not the fuse.... (I will buy another one from Maplins tomorrow!)As I have written elsewhere both the Mill and the Lathe are very nice pieces of equipment -but the quality of just a few of the components could do with some examining. To replace the fuse holder is not a difficult job -it is however very fiddly and to be honest it not something I feel like doing at the moment. SO, the pieces of steel that have been cut to size are the bogie side plates and just one side of the lower cross member for the central power chassis. The vertical worm shaft will be held in position by the upper and lower cross members. At the top of the vertical shaft will sit the reversing dog bevel system. This part of the drive system is at the “I know how it works -but how do I get it to work?” stage of operations. In theory all I have to do is slide a shaft to connect with a forward facing bevel and then slide it back to connect with the reverse bevel. Thus the shaft still rotates in the same direction but the take off is in one of two directions. The shaft will have to “lock” in a Forward Neutral and Reverse manner. This is going to have to work from a sort of “notched” pyramid shape. The central notch will have to hold the slide shaft centrally clear of both bevels and then lock it solidly in either fwd or rev. All this now has to be interlinked to the pump from the torque convertor so that the pump fills the convertor in the Fwd/Rev whilst it empties in the chamber in the Neutral. Time for some serious brainstorming  and an ample supply of tea!!!

Believe it or not less than 24 hours after having placed my order (via my wife) over the telephone my castings arrived on the front door step held by a very pained looking Postie... The castings are of very high quality and errrm -they weigh a tonne!!! Well perhaps not that but the larger ones come in at 450 Grammes and the smaller ones at just under 350 Grammes. Since this is a 2-D-2 loco the poor Postie must have had a hernia carrying the crate from his van up the garden path.

See Picture 18.
See Picture 19.

I have the new fuse holder from Maplins -but it is going to have to wait until Thursday Afternoon at the earliest because of domestic commitments. I will have to move “Dobbin” out of the shed and then cart the Mill to the kitchen -where there is plenty of light. Fortunately this is not too far but at 35 Kilogrammes weight it will probably feel as far as the distance from the front gate to my door for the Postie.... Then it should be a simple case of unscrewing the control panel and then fighting through the tangles of cabling until I can get at the back of the fuse holder to unscrew it and solder a new one into position.
 
Having played “Mr Fixit” with the Mill I can now get back to work....

Well over the past couple of days I have been busy, some of it to do with this loco -but quite a lot of it to do with my fettling my sons bicycle.... The next shot shows the Mill with its vice clamping the work piece safely. (D.Ennis Esq please note). The ends of the plates are now “square to themselves” and as far as I can tell  exactly square as well!!! The stack of squared off primitives now await the scriber and rule for their holes.

See Picture 20.

While this has been going on I have been having a “practice” with one of the wheels. I have never “done” cast iron before and I thought it an opportune time to have a go with it. Having spoken to “them as does” to quote  a Southern Derbyshire friend -I changed the jaws of the lathe over to external and then fitted the wheel casting in -nose first(?)

See Picture 21.


The cutter then passes over the rear of the casting to produce a flat face. This is a vile operation as all the black iron dust clings to any slightly magnetic object and soon the lathe resembles a magnetic iron filings demonstration in 3D.... A few flicks of the trusty paintbrush and things are again visible. The now flat face is needed to clamp it against the face plate, (to be used later). The next operation is to centre bore the casting. The next shot shows the Slocombe fitted to the chuck about to start boring. I have always found the double ended Slocombe drill to be a very strange thing to look at!!!

See Picture 22.

Monday Evening. All of the Driver wheels have been faced and drilled to M6, there are 3 Bogie wheels still to do and to be honest my “eyes” have gone!!! However I am not displeased with the evenings work and the stink of hot iron chippings has almost certainly killed all the bacteria that may lurk in my shed... I have found cast iron to be remarkably easy to work on -bar the smell and chippings that seem to somehow get everywhere. Do I prefer cast iron wheels to the ones I normally make from steel?

Well the answer really has to be no.

For ease of machining and gripping in the jaws of the lathe steel wins hands down every time. I worry that pieces of the castings are going to fly off whilst I am machining them. One actually did on Sunday Afternoon and although it was not very large, it left quite an impression on the safety shield...

Wednesday evening. All of the wheels have been faced and the flat faces bolted together. Some “fun and games” were had as I machined off the casting “buttons”. I had originally intended simply to pass a cutter around the end of the casting and thus cut through the button leaving a ring of cast iron to be disposed of. This worked -sort of... It did in the end prove to be simpler and quicker to knock off the spare cast iron with a  cold chisel and then turn the complete wheel as a pair of ends. Something to remember for the future.

The next problem that faces me is the axles for these wheels. I think that I have some silver steel rod of the correct diameter but I have always found silver steel to be very difficult to machine and in this case I think I will have to order some mild steel rod to make them from. The bogie wheels will have to have an allen cap head bolt fitted to the non rotating axle shaft as this is what the floating bearings will be mounted onto (see the NER EE-1 for more explanation). The drive axles will be 8mm turned down to 6mm for the wheels and the bearing for these will be in the horn blocks. Fixing the drive wheels to the drive axle is going to be “fun” as well. My best option is the drill and tap an M3 hole in the wheel boss and then use a grub screw to secure it to the axle.

Thursday Evening. I have begun to prep up the wheels for their finest moment. The first step is the face the fronts of the wheels. The next shot shows a driver wheel in the jaws of the lathe.

See Picture 24.

The next shot shows a bogie wheel still with its button casting. The axle hole will be enlarged by 0.5mm  and then an end mill will be used to cut the “blind hole” for the ball race to fit into.

See Picture 25.

This shot shows the tread for the bogie wheel being cut on the lathe. This is actually very easy to do as the button allows me plenty of room to get my cutters into position.

See Picture 26.

Unfortunately the same thing cannot be said for the driver wheels... These have had to be mounted on a coach bolt and then “nutted up” in the jaws of the lathe. This does work reasonably well -despite the chattering of the cutter. But the main problem is that the jaws have to be tightened up so much that it destroys the thread on the bolt....

See Picture 27.

Well a few days later and all the wheels have been “roughed out” on the lathe. They are now the correct size for loco the bogie wheels have come out at 48mm and the driver wheels have (just!) come out at 60mm. I will admit to cheating like mad and using part of the button for the flange for the drivers -however I have (mostly) got away with it. There will be a couple of “dings” in the flange edge -but this would have happened anyway with wear.... (he says....) So, at the moment all the wheels are set for machining the flange angle and the coning on them. This means using the one piece of equipment I have for my lathe that I really HATE!!!

This is the Compound Slide.

It is a very simple piece of equipment but for some reason it seems to delight in; fouling the saddle, bashing against the tail stock, or being in such a position that it is impossible to fit the cutter to the work piece, or, (its favourite trick) of being just right to foul the chuck/faceplate at almost the end of the cut...

Here you can see the slide set up for cutting the back angle of the flanges for the Driver wheels.

See Picture 28.

I have been going through the suppliers catalogues for suitable bearings for my Bogie wheels and there is only one real choice... This is a bearing of the tiny type! It is 8mm diameter with a bore of 4mm and a width of 3mm -as is my norm I intend to get it from Technobots. They stock it as part number 4255-122 at a not unreasonable cost of 65p inc VAT! The load is a little light for my liking at only 395 Newtons -but spread over four bearings per axle it should take the strain. I know the STATIC load would be over 40 Kilogrammes but the DYNAMIC load is far higher. This will mean boring “blind holes” in the Bogie wheels to take the bearings and some “Loctite Green Sleeve Retaining Compound” to hold them in place. I have no idea what that stuff is made from -but it has held together things that I would have never hoped to stay together for durations that I would have called impossible!!!

The bearings for the Driver wheels (part number 4255-182) that will have to fit into the horn blocks are of a similar loading at 1,252 Newtons. Alas they are 16mm diameter which means that I am going to have to unship the 3 jaw and hernia on the 4 jaw and take out the 12mm hole to 16mm with a boring bar. I like the 4 jaw but its icy cold 2.5 Kilogrammes is slightly awkward to “nut up” whilst held up by two fingers and a thumb...

Tuesday evening. The work on the wheels progresses and now I have (finally) 8 Driver wheels ready for final mangling... The off set inclined hole for the grub screw has yet to be done and I will admit that I am not looking forward to doing it. I have used this time to experiment and apply my own personal theories.... Well it is my model so I am allowed to. I accept that the standard coning is 3 degrees and all but four of my wheels are cut to this. The outer drivers are cut to 5 degrees as this (I have worked out) will give me “just that bit more” cornering ability -something that I need on my tight curves

The Bogie wheels have come along in leaps and bounds and all that they require doing now is the coning and the flanging angles cutting on them. I have bored the “blind” holes for the bearing on each side of the Bogie wheel. This was a truly nasty operation as the Slocombe insisted on clogging with iron dust and and having to be withdrawn from the work piece and blown clean -thus covering everything (and me) with fine iron dust... Once I had got a lip of about 1mm I could then change over to the end mill and bore down the hole to provide a flat bottom to it. This was very quick easy and (I am told) unbearably noisy!!! I bored in 5mm deep on each side of the Bogie wheel and I decided to take out the centre hole to 6mm while I was there. This will provide a good oil reservoir when I assemble the bearing.

The next shot shows the Bogie wheel being bored with the end mill. If you look at the two bogie wheels on the saddle you can see the bore holes on either face.

See Picture 29.

The same procedure is (I think) going to have to be done when I start producing all the carriages and wagons that I will need. Despite, “certain persons”, claiming that my locos could pull a house around my garden, I  think that the use of fully floating bearing into my rolling stock will produce a more nicely behaved item. This will mean that instead of relying on the coning to provide the difference in radii (and hence linear speed) The wheels are free to move at differing rotations. This will place more load on the flanges as the steering effect will mostly be down to them -rather than the continuous “sliding down the coning” that provides the side thrust to the axle.

Now that the wheels are almost finished and the shed is getting rapidly colder.... I have been sat near the cooker in the kitchen working out things from my old text books. I have an old book from the company PIPER FM ltd that has all the formulae in it, (called not unnaturally the PIPER TUNING MANUAL). I will confess that I am not sure if the company still exists(?) however it does explain the reflection supercharging of a 2-stroke exhaust system -probably better than I am about to! When the exhaust port opens a shock wave travels down the exhaust pipe. As the shockwave expands it slows down and draws the exhaust gasses with it and pulls clean air and fuel with it -hence the first cone section. Then it travels at a speed along the straight section (the length of which is time dependant) when it is compressed by the second cone section and exits the exhaust system. As it exists the exhaust system a secondary shockwave travels towards the exhaust port of the cylinder and pushes BACK any clean air and fuel as the exhaust port closes. This then adds to any shock wave charging from the inlet side of the cylinder...

I hope the diagram below helps to explain!!!

See Picture 30.

The length of the timing cylinder is dependant on 2 things; the speed of sound and the contents of the exhaust gasses. The speed of sound through the gasses increases as the temperature increases -but (Ha Ha!) not in a linear fashion... The content of the exhaust gasses depends on what is being burnt... Fortunately the book contains three sets of tables from which I can “perm” my exhaust gasses. One table contains Nitro Methane mixes, another Petrol mixes and finally (thankfully) Methanol. I know that what I am going to burn is NOT “Straight Methanol” but this is the only data table that I have -so I will have to use it (and abuse it!)

Based on my design for the convertor I have to pump in figures that will force the system to supercharge at my desired rotation -8,000 RPM I end up with an impossibly big exhaust system with an infinitely thin timing cylinder 48mm wide and the system is 478mm long!!! For obvious reasons something is going to have to “mangled” -seriously. The best bet is to fit the exhaust system with some form of cooling fins to lower the temperature of the gasses and then to force cool the fins. The draught from the radiator fan should do nicely and the fins will provide structural strength, rigidity and something to bolt it all into position with...

If I can cool my gasses using the coolant water then things become manageable -but the heat still has to be dumped via the radiator. The best bet would seem to use the coolant water from the cylinder head to cool the gasses as they enter the expansion chamber. This would mean using a co-axial tube for the “Header” section from the exhaust port to the start of the expansion chamber. This cools and (more importantly) lowers the speed of sound through the gasses. Curiously enough this does not affect the length of the system -but it does cut down on the width of the pipework and I can now use more “delicate” 15mm pipes.

The Resonator chamber is going to have to be build in sections -or built as a core with end flanges -I haven’t decided yet. Each “chamber” of the Resonator has to be 1.4 times the volume of the previous one -this has to do with the adiabatic modulus of the air and the pipes are very “flute like” in their construction. There have to be holes drilled in the walls between each part of the chamber that are 35% of the surface area and the whole lot internally “lagged” with some form of dampening medium (probably glass fibre!)

A couple of evening at the calculator and I will admit I had to unearth a teenage “A” level Physics text book that (errrmmm....) never seemed to have got returned to my old grammar school at the end of my upper 6th form(!) At the end of the maths and the brain creaking with node and anti-node plus reflection and constructive and destructive interference I have emerged from the trauma with the following rather large full scale drawing.

See Picture 31.

Now, this is an ideal drawing- and not a real world practical one. I cannot see how I could possibly fit that lot into the loco shell along with the tanks and pumps etc that are already having to be shoe horned into it!!! The first part (going left to right) is the expansion chamber. This is a “Brooklands” type which gets its name from the race track where they were first used. They are very simple to work out, having a 45 degree expansion cone and a 45 degree compression cone. Being a lazy mathematician -guess which angle has a tangent equal to 1.00? Being of a “flat” design rather than conical -this removes Pi as well.

The specifications for a Brooklands Silencer are pretty easy…

The exhaust gasses are lead to a chamber that is:

"Of not less than SIX times the swept volume of one cylinder. The diameter D (if cylindrical) being not less than ONE FOURTH of the length L , the tail pipe shall have an internal diameter not more than ONE HALF of the equivalent diameter of the silencer"

(Don’t you just LOVE the 1920’s English!!!)

The inlet pipe has perforations along its complete length as well as being open at the end. The shock wave then hits the 45 degree end and gets bounced back on itself. The exhaust pipe from the chamber is similarly a length of perforated pipe open at the end. This type of expansion chamber has one serious flaw -it produces the “bark” like sound that is so characteristic of old time racing cars.  The resonator chamber is similarly a classical design from a racing pedigree -this time Bugatti... The inlet pipe has perforations on the top facing the curved part whilst the exhaust pipe has perforations on the bottom facing the curved section. Both pipes are open at the ends.

Whilst it is well known that Bugatti came from a background of furniture making -he also liked music...

The five chambers damp out the frequencies generated by the ”Brooklands” expansion chamber. The effective length of each being 1.4 times that of the last. Between each each pipe there are loosely packed glass fibre strands to break up the shock wave and render this to a pressure flow across the chamber.

So far so good. I now need to do some real world investigations as to the exhaust temperature etc of my engine and the water temperature that will result from water cooling the exhaust manifold. Hopefully at the end of the experiments I will have some hard data to plug into my dimensions and end up with a somewhat smaller exhaust system!!! The design is based on a gas temperature of 450 Kelvin and even if I can only knock down the exhaust temperature by 20 Kelvin -I can shrink it by 25% due the lowering of the speed of sound.

Some mangling with the Universal Gas equation, ((P1 x V1) / T1) = ((P2 x V2) / T2) , produces the volume of exhaust gasses that the motor produces based on its RPM and the temperature at the start of the exhaust pulse. This is as yet “simply theory” -as I have yet to push a pyrometer down an exhaust tube. Similarly it produces the pressure at the point of exhaust thus the peak shockwave pressure into the exhaust system.

Due to the Mill not behaving itself, the work has slowed down to a crawl... I have had to unearth my pillar drill from it’s hibernation. Admittedly this is something that I would have had to have done anyway as the holes that are now required exceed that of the chuck of the Mill. The next shot shows the four side plates of the traction bogies aligned in the vice with a 3mm drill to punch the initial pilot holes through the plates. The stack is then taken to pieces and (hopefully) the pilot holes will align the 8mm drill that is the next through them.

See Picture 32.

After having produced the first set of plates and fettled the holes to the a nice shape (de burr etc!) I had a trial run with a couple of 8mm nuts and bolts then roughly gapped the wheels to the correct back to back setting. I had a big grin on my face as they rolled smoothly along the piece of track plonked on my stool and then clonked onto the lino floor of the shed as it fell off the end.

See Picture 33.


They moved so smoothly the question I now have to ask myself is :”Do they need ball races?” The answer I am afraid has to be “yes”. Even though they move well, they are moving without the frictional weight of the loco on them, this may result in a great deal of problems that will not occur if I use ball race bearings... This does mean that my nice 8mm nuts and bolts are not redundant until I get the 12mm drill out and bore them to the correct (outer) diameter to take the flanged ball races.

Another thing that may alarm people is the the use of fully floating compensated bogies -I intend to use these for my traction bogies as well as my leading and trailing bogies. These will be rather more “robust” than the more flimsy type commonly associated with carriage bogies -but the principle will be the same. I am not the first to use this in a mainline locomotive, several Russian steam locos of the Stalinist pre WW2 era also used this type of compensated steam bogies. But, this was probably more to do with the appalling track conditions due to winter and summer movements that would have snapped springs etc.  There will be torsional springs across the traction bogie to force the wheels to follow the bumps, (hopefully not that many!), that it will encounter.

There will be an 8mm threaded rod from one side of the bogie sitting in a 8mm bore steel tube from the other side of the bogie. The threaded end will be sunk into the tapped hole in the plate and silver soldered there. The tube will be welded to the other plate. I will bore an oil hole in the top of the tube to admit some oil to the threaded bar and “keep it sweet” as we say around here!!!

Due to the appalling weather I have been forced to spend a morning (or two) in the shed (shame!!!) Armed with my sticks of “B6” and “Easy Flo2” I started assembling the bogies (of both types). Having unearthed my “hearth” from the shelf I then put the 4mm bolts through the holes and nutted up the other sides -being careful to apply plenty of pencil lead to the thread before I did so... When silver soldering steel I tend to use MAPP Gas -which I like -despite its evil and disgusting smell. The ends of the bolts glowed a nice red and the B6 clung lovingly to the steel and then flowed around the bolt head. Before it could get much further I threw the flame to the next one in line and continued along the line until they were all done. The next step was to change over to Propane and then affix the bolster between the two plates.

See Picture 34.

The reason I switched gasses and solders has to do with the differing temperatures of melting of the two solders. The cooler Propane cannot reach the temperature needed to melt B6 -thus the bolts remain firmly fixed and will not fall out... The bolster was held in place by the simple method of clamping it in place with a very long M4 nut and bolt (which also held the side plates vertical-ish). I will be the first to admit that I do not like Easy-Flo2, I find it far too liquid -but on the other hand this extreme liquidity is just right for getting into the gaps between the plates. You can see how it has just SPREAD everywhere along the joint -but it has penetrated right through the gap to the other side. So, typically enough for me -the joint is ugly but strong!!!

The next shot shows the rough assembled bogie.

See Picture 35.

Here you can see the bearings inserted into the left hand side wheel -the stub axle nuts up nicely(!)

See Picture 36.

The next step of operations is to start assembling the traction bogies. The plates were bolted together as seen below. There were I will admit a few panic stricken moments as I had to really check that I had all the pieces in the right order -not only are there a right and left there is also a mirror positioning because of the fully floating aspect. (Check once twice -maybe again???) In the sure and certain knowledge that if I got this wrong, I screwed it up royally -I hit it with the MAPP Gas and B6.

See Picture 37.

The product of my labours -a slightly rough collection of wheels and plates.. However I am not displeased with it as you can now see the basics of the locomotive. This is a first for me as my normal method is to build the bodywork first and then cram everything into it. It feels very strange to look at the naked bogies!!!

The next problem on the horizon is to weld the frame that will form the base for the bodywork. I have most of the square section tube cut to size, (bar some filing!) -they are going to have to be “self jigged” welded together. This is a strange, almost “ritual” like procedure, in which opposing ends and sides are welded and allowed to cool before the next stage commences. I am going to do a “belt and braces” setup and join the corners together with some “pop” rivets that will take some of the stress off me as I just know that I will disturb the layout when I fumble around in my welding helmet!!! Once I have a tack weld in each of the joints than I know that I am “safe” -but it is the bit before that....

Well as they say “these things are sent to try us”..... After having drilled all the 5mm holes in the steel tube and located my pack of 5mm pop rivets I duly cranked the gun into the hole crunched up the rivet and “THWUNCCHHH”. “This”, I said to myself, “is not a good sound”... Sure enough it wasn’t. The pin had bent inside the rivet gun and jammed it solid. The next two hours were spent persuading the rivet gun to come apart. However by dint of brute strength, dire threats and main force I got the thing apart and lo and behold -the spring had broken. Thus the tension on the jaws was never removed when the barrel moved forwards. I duly replaced the spring with a couple of new ones from my “box of bits” (where would the world of modelling be without a “box of bits”???) and then in under 5 minutes I had the thing back together...

The frame is now ready for welding.The aluminium pop rivets will, I know, melt when the steel welds -but by that time they will have done their job. The next shot shows the rough assembled frame. There are only two really critical measurements that have to be held “true”. They are the centre lines for the frame -the rest of it can be “about there” as most of it will be hacked to fit the components and brackets that will hold tanks and radiators etc.

See Picture 39.

Another thing that I am starting to look at again -is the final connection from the gearbox to the drive axle...

I had intended this to be a vertical worm wheel to a spur gear on the axle -but this is starting to look increasingly vulnerable to; dirt, grit and the odd piece of herbaceous border plant with a name always seemingly beginning with an “H”... My new option is to drive the axle from a toothed belt from above. This does have the added benefit that it keeps all the vulnerable parts of the drive chain above the dirt line and the toothed belt is fairly coarse so muck & “H” plants etc will not really hamper its operation. This will entail producing a floating platform that will move in the same axis as the bogie, (this is not much of a problem!), and a flexible joint that connects the drive from the reversing gear system to the platform which will also be fully floating along with the bogie, (this may require some thinking...)

Well after a couple of nights sleep, (I have also not been too well -cough cough!), I think that I have most of the new drive system worked out. Everything remains as it was in the original setup -just that the worm dive is now inverted and drives a spur gear above the chassis plate. This is going to require some 4mm pierced plate, (it looks like sheets of “Mecanno”!), to be assembled and soldered into place.

Having returned from the shed covered in Paxolin dust from sawing the base board for the loco I return to my thread. Why Paxolin??? It is oil and water proof, cuts with some difficulty and it is rather strong -plus the fact that I happen to have a large sheet of it in the shed left over from building the Krokodil... The 3mm sheet was duly chopped to 12cm by 64cm and most of the saw marks filed off it. It does not have to look too pretty as its primary function is to be: drilled into, glued to, screwed to and generally abused -during the life of the loco. Its secondary function is: to stop things falling onto the tracks(!)

I have scored a centre line along its length, and now that the base board is there I can doodle onto it the positions of all the bits and pieces -that have to fit there. Some of the shapes for the tanks that I am going to have to build are “not pretty” and I have resigned myself to the fact that both the oil and water pumps are going to have to sit at the bottom of the tanks and be driven by long shafts from overhead motors. This makes the construction of them a little awkward as to examine what the pumps are doing will mean that either I have to make the pump out of transparent material (PolyCarbonate) or I simply “trust to luck” that things are going around as they should do... People who know me know that “luck” is something that I devoutly disbelieve in. However, the innate perversity of situations, the vile nature of happenstance and Murphy’s Law are things foremost in my credo system!!!!

The tanks for the oil and water are going to be a problem. Although I have a 30cm “fabricator” (bend/cut/roll) I have never really used it -other than to make square and rectangular plant holders for the greenhouse. The tanks are going to have to made from Brass or Copper sheet and this then silver soldered together. I have a feeling that I will be fighting over the cornflakes boxes for supplies to attempt my tank designs with. Some of the “joints” are going to have to be hand beaten with a dolly and planishing hammer to get the seams smooth enough for the solder to creep along the joint.

Decision time for the motor is coming.... Do I buy a 0.91cu (15cc) motor or a 0.46cu (7.5cc) motor? The maths says that a 0.46cu motor is perfectly adequate for the job. However I favour the larger motor on the factors that: it being the larger motor it will be less stressed throughout its life and thus never have to get into high rev situations and (being the larger motor) it is Guaranteed to be powerfully enough!!! The price difference is not that much either, £80 buys me the big 0.91cu motor and £65 the smaller 0.46cu motor. Ok it may be £15 that I have wasted, but then I have not gambled £65 -and lost!!!

Having ordered it over the net the winner was the ASP 0.91m motor. It is big brutal and honestly weighs a lot. Now that this final part of the design is in place -but where do I put it??? Delivery will be in the first week of December 2010 (3 weeks time) and probably by that date the shed will be too cold to sit in for any length of time and static engine tests will have to be done in the lee of the kitchen door -despite pleas of the cold draught coming through the open doorway....

After running in the motor the first job will be to accurately measure the heat generated by the cylinder head by means of a constant flow calorimeter experiment. This was one of the “nightmare” experiments of my “A” level physics years. Measure the temperature of the cold water going into the electrically heated calorimeter and measure the temperature of the water coming out of the calorimeter. Measure the flow by counting the number of drips per minute. However adjusting the flow of the water to get a constant drip rate across the device was the nightmare. However with a home made pump the rate of flow can be adjusted with rheostat(!)

The next week is going to be interesting... I get to weld up the frame for the power chassis and stick the Paxolin to the frame. This is going to mean boring 3mm holes in it to nut and bolt it to the frame whilst the epoxy sets, which despite the name of it, it always seems to set in 2+ hours! I will then bore through the holes from the piece of flat plate that forms the traction bar between the two traction bogies -thus giving me my Beugnoit lever array and the two sets of 3cm rubber blanking grommets that produce the fully floating suspension for them.

Having been shopping for welding supplies and almost broke my hand carrying a “carton” of welding rods home. I had a look at the previous “carton” and it weighed in at 500 Grammes not 2 Kilogrammes. I am not a wimp -but the tube that they are supplied in is just too large for me to grasp easily whereas the 500 Grammes tube is an easy heft with the grip I can get on it... I got a new welding hood -not because the other one was defective -just bereft of modern frills. My son is (I know) want to go and watch Daddy at work -so a “suitably modified” welding hood will be used as a deterrent. The welding glass will be very dark..... (Almost opaque in fact!!!) Boredom will soon do its work. I had to get a new set of gauntlets -the previous set (a fetching shade of red) were grabbed by my wife for gardening in. She does have a point though, not even the most sharpest of rose thorns was able to pierce them. However it does render them useless for welding in...

So, all in all we are ready to roll as they say. The one problem is the dinner party that I have to cook for tomorrow -thus it will be Thursday at the earliest before I can play with my new toys.

Due to the infamous English weather it is now the weekend and I have still to set rod to steel... Somehow rain and arc welding is not a good combination. I am always reminded of the scene in the graphic novel “Watchmen” :) where Rorschach is imprisoned and kills one of his attackers who is cutting through the bars with a plasma torch by smashing the toilet bowl and cistern. The attacker is then electrocuted by the flooding water hitting the cables...

Quote :)

“Never thought of disposing of human sewage with a toilet -obvious approach really...”

Unquote :)

So I have been shopping at the Warley National Model Railway Exhibition at the NEC for the gears and cogs that will form the basis of the transmission side of the loco. I found them on the Squires Stand -which is always the stand I visit last as it is normally at this point I am the most poorest and I feel that I really cannot buy much considering how much I have spent already. Sometimes it even works(!)

See Picture 40.

The small 12 tooth spur gear is the “output” from the front reduction gear chain of the torque convertor. This then drives the 60 tooth spur gear to which is coupled the first of the four bevel gears. These form the fwd/rev mechanism and the output from the bevel directly opposing the 60 tooth is then fed via two U/Js (not as yet bought) to the worm gears. The worms then turn the 45 tooth gears which drive the 10 tooth cogs and then via chains drive the 20 tooth on the axles. The chain is of the self assembly type and four sections are required to be assembled to produce one “link” in the chain. As my wife said “this is something for long cold winters evenings when there is nothing else to do”.

The first bevel is bolted to the 60 tooth by four M2 nuts and bolts and the bore hole is enlarged so that it sits on a length of brass tube that slides on the output shaft -but does not grip it. The “cruciform” bearing for the other two bevel is, (I think), going to have to be made from some scrap Aluminium bar that I have. The carrier for the outside of the bevels is going to have to be machined from polycarbonate. This will have a gear wheel bonded to it. This will form the ”reversing pawl” that will lock the transmission solid when the loco is not moving backwards. The “reversing pawl” will only engage when the “parking pawl” has engaged locking the transmission. Similarly the “reversing pawl” will have to disengage before the “parking pawl” when the loco moves forwards. I have a sneaking feeling that I am going to have to construct some “truth tables” to get everything to operate in the correct sequence. Fortunately I do have a few solenoids left over from the bulk buy I needed to do for the NER EE-1...

OK. Having sat down with a pot of tea some serious brainstorming has had to be done... As far as I can tell EVERYTHING has to be linked to the main servo that controls the throttle. I need at least two “takeoffs” from the same channel. The throttle linkage has to operated via an eccentric thus regardless of the direction that the servo turns the throttle cable is still pulled. The next bit is I am afraid -simply weird.... I have a duplicate servo that turns a series of cams to micro switches and at the and of this there is a sector plate with contacts. Hopefully the drawing below will explain some of the madness.

See Picture 41.

Monday Morning... Well it dawned bright and dry and I was hopeful of finally getting some welding done. I unlimbered my workmate, clamped the frame into the vice and put my foot on the trigger plate. Then the mains power in the house went out and the burglar alarm sounded... After having reset all 16 of the RCBs(!) I dug out my trusty black “smiley” model 8 AVOmeter and put the probes across certain terminal taps. The windings in the transformer core had broken and there were at least four taps that shorted to the PE connection... My much loved green Oxford was now 25 Kilogrammes of oil filled steel and copper scrap. I should not really complain. It was after all older than my wife. How it came out of the BREL works in Derby I have no idea, but it was fixture of my childhood and we all learned to weld with it -even my sisters...

So after a little research on the net and a nibbled credit card I will have to get a new one -probably from “Machine Mart” as they are practically next door to the school where my son has his extra-curricular science lessons. So it will be dump the child and then dump the welding plant into the back of the car and then position it in the shed -just in time to collect the child....

Monday Evening... Well I have a nice shiny new welding plant which is going to have to be classed as my Xmas present to me! It is a nice shade of red, which my wife finds visually more pleasing than Hammerite green. But she is still not too sure of the 400V connection plug! Tomorrow I will start (hopefully) to use it with avengence. Some of the parts are riveted into place and require seam welding and others will require “persuading” to stay in the right place whilst I hit it with the rod. I do have a few NIB magnets that can be used to hold the steel pieces in position... These have the added advantage that they have a very low Curie point of 80 degrees Celsius. At higher than this they cease to be a magnet and will drop off the hot metal. I used them this way some time ago and although it worked perfectly, I did have to lever off the NIB magnets from the steel toe caps of my protective boots...

Tuesday Morning... Well everything worked bar the expected problems of the learning curve for the new plant. The dial indicator is only a “judge” rather than the “specific” taps of the Oxford. So I started off with around 60 Amperes and worked up to what the indicator on the slug said was 80 Amperes. At this point the arc held true and steady as it would have done on the 60 Amperes tap on the Oxford. The welding is rather messy, even by my standards -but it does hold everything together.

The central strap for the traction bogies has ben unified with the transverse pieces of square section tube steel and then the hole lot joined to the rectangular frame. I did not in the end bother welding up the end pieces as they seem to be quite happy with the rivets. The next step is to dig out the angle grinder and make things look pretty prior to paintwork.  Yes -it is going to be Hammerite green. Well I have to use it up somehow now....

Tuesday Evening... The rolling chassis is now complete -all I have to do is power it!!! The leading and trailing bogies have been positioned with their M4 pins and arms -but the transverse tensioning with springs to force them into “guiding” the loco has not yet been fitted (or even worked out!) The traction bogies have had the M6 bolts that are their pivots welded into place at the bottom of the U. Slight “adjustment” will have to be made to ensure that they sit perfectly vertical, (pass the hammer). The sheet of Paxolin has been drilled and bolted to the frame -it awaits daylight for the rubber grommet treatment, (my eyes have gone!) The chassis has been tested on the sharpest curve that I have and nothing binds. The tensioning spring between the two traction bogies may be a little weak for the job (?) but it provides enough tension to force the traction bogies back into alignment after exiting the curve. One of the most annoying aspects of the day was the discovery that my nice beautifully machined cast iron wheels where now starting to to show slight but definite signs of RUST. Time to move the chassis out of the shed into the warmth of the kitchen...

See Picture 42.

Wednesday Morning.... I should have moved the model into the kitchen last night(!) The temperature in the shed fell over night to minus 2 degrees C -thus the steel of the model was “sticky” to my fingers and quite frankly painful to touch!!! So, after having disassembled the rolling chassis from its curve to the piece of board on the cooker to warm up. I dutifully covered everything splashable with pages from The Express, I dug out the first pot of primer that I reached. Typically enough it had this nice crust on it -of ice... Time for more tea! Once the paint had thawed I stirred it and slapped it on. It does look rather more attractive in the photo than real life. The nice red colour dries to a mud brown. But since the last loco that had to be primed prior to painting ended up a fetching shade of beige when it dried -I don’t think this really matters as it will all be dark green soon.

See Picture 43.

The first parts of the frame have been painted green and are drying over night on the cooker (which has been well stoked for the coming cold night!)

As the motor is due sometime in the next week, I have sat down and begun playing with pieces of cardboard to find out where everything will sit. Breakfast food cartons are cheap(ish) and they take several rubbings out before I wear a hole in them(!) What the cardboard cutouts have shown me is that the area that I have to play with is even smaller than I thought. Some of the gears are going to have to be mounted directly onto the sheet of Paxolin and I plan to use the 4mm perforated steel strapping to provide the spacings for all the gears. Once they have been secured then I simply bore through the holes in it into the Paxolin and everything is rigidly mounted (hopefully!!!)

The nasty that has arisen is the expected problem of changing gear...

I had hoped to be able to do this with just one set of dog bevels but no matter how hard I fiddle with the layout I end up needing two sets... Likewise I was originally using one solenoid -but now I have to have two.

But, all is not doom and gloom as it might appear. This does make the solenoid a simple pull-pull fed by a DPDT relay. The gear shift will resemble a slotted plate that is pulled forward and backward by the two solenoids -not unlike the standard set of points motor used by my son’s Hornby.

The cardboard also reveals the positions of the tanks -and it is not a good one. The shapes that they are going to have to have are dictated by the volume that I need to store in them and the pump that is going to have to sit at the bottom of each one. The tanks are going to have to sit towards the radiator end of the loco. This was rather expected -but it does produce plumbing problems. The torque convertor will require a drain back to the tank -this means that the drain will have to exit above the surface of the oil -it will do this via a “Swan Neck”. The pump will pressurise (slightly) the torque convertor and there is the “environmental problem” of an oil leak. This also means that I am going to have to figure out some form of oil seals for it.

“How do I start the motor?” is another problem starting to rear its head. I have a plan in which I extend the motor drive shaft out past the end of the torque convertor to a hex end. This connects to a battery drill fitted with a over run coupling. The idea is that I power the drill and the motor starts. The Glow Plug will I feel be of the “permanently live” type, in that it will have a current running through it all the time.

Normally Sunday Morning and Afternoons are times when I am very productive -however due to the incredible cold snap that we are having this means that I am keeping warm in the kitchen -so work will slow down -but  it will be nice and warm....

This particular Sunday Afternoon was spent in the kitchen on the floor mat -near the cooker...

I did some trials with the positions of gears and shafts. The first shot shows the initial trial on the piece of Paxolin.

See Picture 44.

The next shot shows the provisional working arrangement. This is not as “elegant” as I would like -in fact it could be quite difficult to service. However, I feel that this is the correct arrangement for the system as it can be manufactured in modules and then “layered” together. Moving the worms towards the centre of the model allows me to fit a larger gears to the “input” shaft.

See Picture 45.

Most of the day has been spent sitting at my drafting table and abusing sheets of graph paper... It is amazing how thing conspire to clash against each other when you start to draft up the arrangement. I was sure that I had enough room and yet, despite my best efforts, I had to screw up two drawings -the sum of three hours work.

I have also found that my self assembly chain may be the only length that I ever buy. Tedious is not the word!!! I have assembled 24cm of it -enough to go around one gear and that is enough for one day(!) As with the “Krokodil” there will be a chain link between the power axles and the conrods will be purely decorative.

At the end of the day I do have a drawing with most of the things in the correct position and good idea how the reversing mechanism will function and where it will fit, (this time it will not clash if it knows what is good for it...)

The locking system for the reverse/forward gear is very simple -every filing cabinet has one that works in the same manner. It consists of a plate with two parallel slots with a diagonal with a captive pin in a transverse slot. Moving the plate across the pin moves the pin from one channel to the next and it cannot move back without the plate sliding. The plate will be pulled by two solenoids acting in the same direction and a return spring. This means that if the power fails the default direction will always be forwards. The plate will act on a bar at the end of the two transverse shafts sitting between two thrust bearings and this will push/pull the shaft across the dog bevel to select direction.

Although the gears are nylon I am going to sweat a piece of steel to the shafts and then pin the gears to this with nuts and bolts. Thus the torque will be taken through the nuts and bolts and not through the grub screws on the gear wheels. I still remember the grub screw that cut a neat thread on the shaft when I was testing the gearbox for the NER EE-1...

The arrival of the motor is in sight and I have to give some serious thought as to how I get the power shaft from the front of the torque convertor to the central gears. I had originally intended to use some old powder metal gears -but I now believe that this is the wrong way to do it. So I am thinking of driving things from toothed belts. This will damp down any vibration and hopefully give me some quieter running.

Wednesday 1st December 2010.... Possibly the most successful day ever with this model!!! Although at least 25cm of snow had fallen over night and the outdoors was in the less than balmy temperature I set to work on the kitchen floor. The previous night I had completed drawing №4 of the gearbox and miraculously it seemed to fit al the parts into the right places and nothing clashed (too badly). Braving the cold I stepped out into the white wilderness and retrieved my set of marking instruments and made some hot tea!!! Well this shot shows the the №4 drawing and the transcribed positions on the sheet of Paxolin bolted to the frame. Drawing in 16 pretty colours is normal for me -a 0.3mm felt tip is more transportable than a Unix workstation running AutoDesk...

See Picture 46.

The next shot shows the progress after a couple of frustrating hours. I had to chain drill the slots with a 3mm drill and then “pick” the chains apart with a floor board saw until there was enough room to get a proper saw in there. I had to smooth up the shape first of all with a Rasp, then a Bastard file and finally a half round to smooth it all off with. Paxolin dust of course went everywhere and “Henry” spent quite some time sucking up the mess... Cutting the final slot for the central gear was I admit risky. I nearly cracked the sheet twice -I am going to re-enforce it with some transverse hard wood strips later.

I drilled out the gears to 4.5mm and inserted a CA’ed length of K&S brass tube -giving me a 4mm bore to the grafted gear made from a bevel and a 45 tooth spur. Whilst the CA sets hard over night the grafted gear will then be drilled and pinned in the morning. These stand on M4 bolts that fasten through the steel frame and emerge onto the Paxolin sheet. The central 60 tooth spur gear was fitted to its 4mm shaft and the two worm gears duly bashed along the shaft until the hit the right position, There will have to be a further bracket and ball race besides the gear as the only supports are at the ends at the moment.- and you can just bet the thing will wobble madly without it... All the raw brackets are going to be drilled to take M10/4mm bore ball races.

See Picture 47.

The next two shots show the rough assembled final drive and reversing system.

The blue self assembly chain on the small sprocket is obvious as it vanishes through the slot to the large sprocket on the outer drive axle. The dog bevels are on the shaft and (hopefully) you can see how moving them along connects first with one side and then the other.

See Picture 48.

This shot shows how the input drive from the torque convertor reaches the central gear. The grafted gear JUST misses the shaft by 2mm and the 20 tooth gear drives the 60 tooth gear cleanly.

See Picture 49.

After some discussion via “chat” I have taken the advice of a friend and purchased the 0.46M motor as; “Thats too big an engine for a toy train”, so we will see... The big motor 0.91M is a special order -but the 0.46M is an off the shelf part. I wonder which will arrive first?

If you examine the gearbox drawing at the top of the page then examine the Picture 49 -you will see that the one that I have built is upside down compared to the original. However like the original gearbox it should be pretty smooth in operation.

Well the snow still falls so I spent the day in the kitchen. First job of the day was to strip off all the test stuff from the Paxolin sheet and dig out my bow saw and start sawing up the hard wood framework for the gear box. “Why Wood”? I hear you ask -because it is nice to work with and quick and easy to change things when you have an oops moment!!!

I drilled out the brackets to take the bearing -rather painfully having to “wind out” the hole from 5mm to 10mm a millimetre at a time... I have found it is better to be bored than to twist the bracket. The next shot shows the worm gear with a bracket and bearing. the basic framework for the reversing “Ballista”(!) can be seen in the top right.

See Picture 50.

This shows it all far better. The throw arms sit either side of the central gear and the whole thing is assembled with “Croyd Aero”  and then bolted and glued to the Paxolin with epoxy. After 2 hours I could start again. It may be me but I have found the slower 2 hour epoxies to be far stronger then the 5 minute ones(?)

See Picture 51.

The next shot shows the first assembly of the transverse shafts. The brackets are bolted in place and the dog bevels “tapped” into distance along the shaft. This is tooth plus 4mm -so the “shot” from the Ballista  is 6mm in total.

See Picture 52.

Ok -over head shot. You can see the third bearing on the central gear -this should remove any wobble from it (please!)

See Picture 54.

The next shot shows the end of the days work (and my eyes have gone too) So sorry -I have had to use AutoFocus... I need to ream out the small sprocket to 4mm and start trimming everything to size. I will admit that it has been a very rapid couple of days progress!!!

See Picture 55.

It is still snowing -so I am back to work in the kitchen, (what a shame!!!) The first thing to do today was to construct the gear shift arrangement. This, as I have said before, uses the same mechanism as a set of filing cabinets. The slide is made from a 50mm M3 bolt, (suitably filed), and a length of U section brass. These were then silver soldered together -they will never come apart, (which is how I want them). These now form the pin slide that transfers the longitudinal movement to transverse movement.

See Picture 56.

The next shot shows the pin slide with ABS sheet CA’ed to it to act as a lubricated channel. The pin slides on a I beam section of ABS. A little touch of sand paper ensured that there was very little rattle. The top of the slide is now flush with the arms of the ballista. You can see the 4mm collets that will take the thrust bearings for the transverse shafts.

See Picture 57.


This is the base plate -made from a 3cm length of 1 inch 64 thous K&S strip. The shape of the slot does not really matter as all we need is a 3mm wide line between the extremes of shift. The function of the base plate is to hold the pin slide in its groove as it is pushed and pulled 6mm. A little CA holds it in place whilst I drill down through the arms of the ballista to hold the M3 nuts and bolts.

See Picture 58.


This is the top plate. The nice sections of L brass provide the smooth direction for the movement of the slide pin -regardless of the dire nature of the hole that they are covering... They are held together with a little silver solder and an M3 bolt is used to provide an accurate line between them.

See Picture 59.

The completed top plate. The slot can now be trimmed up with a needle file until the hole at the bottom of the plate matches the slot provided by the two L sections(!) A quick once through with a 3mm drill clears out the holes in the top plate that have been covered with the lengths of L section.

See Picture 60.

The reach rod is at the moment rough cobbled from a few lengths of pine strip wood, (see above!), it has a 60 degree slot and captures the pin thus pulling and pushing it across... The final version will have a short length of brass tube around the pin to provide a rolling surface. The rough version tends to catch on the threads of the M3 bolt.

See Picture 61.

This shows the completed ballista gear change system. The pin has been fitted with a cross arm, a 1/4 inch sq K&S tube, to push and pull the shafts. This will be re-enforced with brass plate in finally assembly. The reach rod is held flush to the back of the gear change with a simple spring loaded shoe, (a length of bent brass strip). This also pushes the slide pin into the angled capture slot. In the final version I am going to have to make the reach rod in two thicknesses and machine out the capture slot. One of the quirks I have noticed is the fact that the gear change is “upside down” -i.e. moving the reach rod forwards engages reverse... The Mk 2 version of the reach rod will have the slots in the other direction. The pencil marks on the reach rod indicate the positions of  Fwd and Rev. The distance between them is 11mm -this is well within the 18mm jerk range of the solenoids. The main problem now is making sure that the solenoids have sufficient power to over come the strength of the return spring and the effort of moving the shafts across.

See Picture 62.


The last day of building before the seasonal madness... I trimmed a spring or two to get the correct rating to hold the pin against the reach rod and then sufficiently strong enough to press the pin into the capture slot. Too strong it made the pin act like a brake, making the reach rod hard to move -too weak and it didn’t force the pin into the slot. So, after taking a too strong spring and slowly snipping off a quarter spiral at a time -I got one with the correct rating to work!!! The screw and swing flap will be replaced in the final version...

The next shot shows the completed ballista with the two “selector forks” I suppose I should call them(?) they are simply U channel lengths of brass with an M3 bolt silver soldered on to them. These sit on the shafts and push/pull the collets. They will be terminated with a couple of M4 washers to act as capture rings & thrust bearing surfaces so they do not slip off the shafts during movement.

See Picture 63.


Ok -now the glossy shots!!! Pulling the reach rod pushes the pin out, the ballista pulls the shafts across, locks it in the out position and the left hand bevels engage with the grafted gear. The pin out position will be the forward position as the pin in position does force the bottom of the grafted gear away from the worm gear, (slightly), whilst the pin out -does the reverse(!)

See Picture 64.


The final shot shows the reach rod in the reverse direction. The custom tuned spring forces the pin and shafts across and the pin is captured by the slot and rammed home into the locked position. The right hand bevel gears now engage on the grafted gear and the loco reverses...

See Picture 65.

Q.E.D. (!)

The next problem is to transfer the filed and twiddled length of wood that is the reach rod into something made of brass. There are, (alas), no suitable K&S sections that can be fiddled to fit -so it is down to the scraps box to supply the parts... I have decided to ditch the idea of a solenoid and return spring and simply have two opposing solenoids switched through a relay. Now that everything works it all has to be taken to pieces and fettled into something that could be called a reliable working device...

After suitable repast I am thinking of ditching the solenoids now!!! The reason is that they are just too fast acting. There is a chance that the pin will not be forced into the capture slot and the whole lot will jam solid. The only other thing is a slow moving linear actuator. This is a fancy name for a nut on a thread!! I plan to drive a 30 tooth Mod 1 gear from a 10 tooth Mod 1 on a small electric motor. The shaft of the 30 tooth gear is, (surprise), a mangled of M6 roofing bolt... Silver soldering a couple of M6 bolts to a length of L section brass strip gives me my arm to the actuator. I will use this to slowly, (but powerfully), move the reach rod through the gear selection system.

OK -any idea where I fit it???

Time for more breakfast cereal packet cardboard...

Sunday afternoon produced the required linear actuator -pretty much as described above. I used one of my many £0.80p each SME motors (eventually I will run out of the box of them?) Opening up the 5mm hole in the bracket to the required size to fit the head of the motor through, required some patience with a broach -typically enough the size is Imperial but the rest  Italian motor has metric dimensions. The nylon adaptor to fit the 3.2mm shaft to the 4mm gear was delicately inserted with a G cramp and the shaft of the motor pressed into the adaptor by crushing the lot in a vice... Don’t knock it -it works!!!!

I lopped off a length of brass and filed a flat square edge on a handy M6 hex nut. A few minutes with a cooks blow torch and they were silver soldered together. A suitable off cut of ABS was pressed into service and the brackets CA’ed to it. Tests with a few kitchen weights proved that the linear actuator is capable of lifting 500 grammes with 12 Volts feeding it.

The acid test was: “Could it change gear?” The hardest part is going from Reverse to Forward selection -so this was the test. The test was done and the answer (thankfully) was: “YES!!”

The place you see it in the following shot is probably the best place for it. But it is going to make the design of the reach rod “interesting” to say the least.

See Picture 66.

Now that the actuator works I have to set the limits of how far it will travel. There are certain points motors that work on the “stall” principle -but I do not like this approach. What I intend to do is to use DPDT relay to provide Fwd and Rev to the electric motor -no surprise. BUT the trick is that I have a Push to Break switch in the feed to the cables to the motor at either end. This means that I have two pairs of cables feeding the motor terminals. The motor turns in the Fwd direction until it breaks the contact and then stops. The opposite direction now has continuity, as the actuator closes the contact as it moves away -so when the relay flips the motor has power to move in the required direction...

I have been playing with card board and the designs that have emerged for the tanks -do not look pretty... I am resigned to having submerged pumps for both coolant and oil. I have decided to go for pure glycol rather than water for my coolant as this is inert and non-conductive. This does mean a bigger tank though. However the tanks can be made from simple tin plate and soft soldered together as the contents will not rust them. I will confess to looking through the IKEA and LAKELAND ranges of plastic food boxes to see if there are ones that are suitable!!!

To paraphrase a famous game... “Colonel Fell”, in the Kitchen, with the X-Acto knife!!! Now that I have a general idea where things are going and nothing is going to be delivered in this weather. The only thing for me to do is to sit by the cooker, make sure it is well stoked, and make my bodywork for the loco. As usual it is a plywood carcass that will be laminated with ABS sheet. I did honestly intend having a “go” with Aluminium sheet -but I feel that this is a little risky for a first attempt -so I am going to have a go with the tanks first...

I also had a “go” with Titebond” for this carcass instead of my usual Croyd Aero -as I have nearly run out. “Do I like it?” Well to be honest -I am not sure... I have several American friends who swear by this stuff -but it doesn’t seem to suit my methods or style of construction. So, all the flat plywood sections are done with Titebond and the laths are all stuck with my remaining Croyd Aero.

See Picture 67.

The strange cross sectional problems reared their heads almost immediately. The windscreen section with the infamous angle was the first victim -it became 30 degrees!!! This made the problem of producing the cross section through the hyperbola that was the roof -a lot simpler...  The square to parabola that is the top of each of the noses I simply gave up on a mathematical calculation and did it by drawing. The laths that form the cross section where simply aligned with the side of the carcass and the angles traced onto them. Some of them are a bit wonky -but since they are just the ribs I am not bothered.

See Picture 68.


After having attacked the collection of breakfast food packets in the pantry I have a template for the bonnets at either end of the loco. The template resembles a cubist version of a cup cake drawing. This was done by measuring the lengths from the curve on the windscreen to the edge at 0.5cm intervals and transcribing this to a sheet of cardboard. The final act was to bend, (somehow), a ruler across all the points and drawing a line through them. The template was then tested and fettled against the curve and I have a template that both fits and works.

The next job was to “roll” the roof. I used a rolling pin, (no seriously!) to wrap the 60 thous ABS sheet around and kept tightening the curve until I got something that wanted to sit on the roof rafters. Then the hard work began... Applying bucket loads of CA to the central rafter stuck the sheet to it. Then by means of brute force I had to bend the ABS to the curve and then tape it to that position. After about 20 lengths of packing tape I had all the edges flush. Pumping in another bucket load of CA filled the gaps at the windscreen ends, (inside and out). Then it was a simple job to mix up some 2 hour epoxy and apply it to the gaps between the top of the side and the ABS sheet. I use about 1/2 of a “double syringe” of epoxy doing this. OK it might be too much, in fact it probably is -but it will hold it firm while I molest it with the sand paper to get a “true” edge to the side. The assembled nastiness is currently “fast curing” by the radiator in the kitchen.

See Picture 69.

In the morning we will find out if I have got a roof and two bonnets -or had an interesting waste of time...

Well the mummification went well and the epoxy had oozed through the gaps and united the roof to the sides. The last thing I did at night was to turn the model upside down and dobbed spot welds of CA along each of the rafters to lock the roof to them. I do not know if this helped(?) but in the morning the model was unwrapped and despite a few dribbles of epoxy I was very happy with the result. There was of course now some “delicate” work with garnet paper to remove the dribbles from the ply wood at one point I will admit to using a rasp! After about an hours abrasive surgery I had smooth sides and square edges. Now it was time for the ABS sheet to come in from the cold -shed... Needless to say they took some time to regain room temperature and their flexibility returned. I have found that it is easier to “crack and snap” warm ABS sheet than cold. When it is cold the sheet is too brittle then the crack can wander from the initial score and you end up with a wasted piece. I used thick CA (which I rescued from my wife!!!) and then trimmed the laminated ABS to fit. At the end of each side I trimmed and sanded each corner square -but there were still the inevitable gaps that had to be filled. I normally use epoxy putty (Milliput) to pack and fill the gaps with. This is very strong and takes a nice finish. The final dent and surface  filling is normally done with Squadron Green cellulose putty.

This Sunday afternoon has been devoted to the cooling side of the locomotive. I scoured the junk draw and extracted an XP1700 heat sink and fan. I know that I saidI was going to construct a tube one -but this is a quickie. I am proficient at liquid cooling computers -so why not use the same techniques to cool my loco? The next shot shows that fan that has been grafted to the Paxolin sheet.

See Picture 70.

More words were uttered as I had to cut a circular hole through the Paxolin by chain drilling it. But it fits nicely. The next step was to measure where the “exhaust” from the heat sink/heat exchanger would vent and then to cut a suitable hole in the correct position. This was then layered with Dacel Plait to act as a grill. The loco is symmetrical and there are similar aero vents at the other end -this is more for show than anything else. The central hole is there because it is there on the original(!)

See Picture 71.

The modifications to the heat sink are as follows: I drilled 3.5mm holes through the base and then drilled 3.0mm holes cross ways to form internal pipework. Into this I epoxied a length of 3.5mm copper tube. The hole lot is then topped with a 2mm thick sheet of ABS this too is epoxied to the heat sink. I now have my thin film radiator. The next step of the operation is to drill and tap M3 into the heat sink through the ABS sheet. I then slap on top of this a sheet of polycarb -this will enable me to see the liquid flowing, (or not as the case may be....)

See Picture 72.

Monday Morning. And as I step out the door I find a collection of packets left there!!! One of them was obviously for me so I opened it and found myself to be the proud owner of a 46 size marine glow motor. I have not studied the motor in detail -just given it the once over and had a look at the instruction sheet. I am happy with the size and look of the assembled bits -so the other motor is going to power “Ixion”.

See Picture 73.

As you can see I have marked the picture to show the various connection points for the plumbing. One of the unfortunate facts of life is that the plumbing points are always in the wrong place -this is no exception.Ideally I would like the positions of the coolant IN and coolant OUT to be reversed... This will make “bleeding” the coolant line harder -and I will probably have to bleed the lines with the engine out of the loco before fitting it. The only position, and one that I planned for it -is inclined to an angle of 45 degrees. This brings the silencer to the vertical and it sits over the gearbox. It is a free silencer and if it works to the satisfaction of the assembled family it may well stay. Failing that I build my own.

The specs for the motor say that it is “timed” for a 5% nitromethane mix and should not be run on less than 18% oil. I personally do not like nitromethane. The combustion products (i.e. NITRIC ACID!) are to me unacceptable. As I said above I am therefore going to use a 20% caster oil and 80% methanol mix. The motor is supplied without glow plug -so I am basically going to pick someones brain as to what would be a suitable starting point.

Having had the motor now for a couple of days I have spent most of them simply looking at it. Not out of admiration for its sheer beauty, but what shape it is and measuring it to within a millimetre of its life... This plus more than a few drawings have shown me that I have to move the centre line of the motor and torque convertor to sit 2cm to PORT. This and the fact that if I change the angle of inclination to 30 degrees gives me a nice corridor to get everything up and down. This way I can squeeze everything into a rectangle 12cm by 14cm. I have yet to fire up my motor, but I have been twisting it every now and then to free it up, whilst slow feeding it castor oil from the same bottle that I use to oil my record player with. It now moves with a polite hiccup at Top Dead Centre and a small length of knotted string has successfully pulled it over at cranking speeds. Things are nearly ready to go!

I have my temporary water pump ready (a Lucas windscreen washer pump) and I need a fuel tank and fuel... The latter is causing me some grief(!) there is now only one supplier of “straight castor” and that is Model Technics. But this is very nearly unobtainable... The Model Technics fuels “GX-5” and “GN-5” both have the correct ratio of castor to fuel but have 5% nitromethane -as does Flair “Yellow”. I might have to explain why the “H” plants are not feeling too well along the  border... Why do I call them “H” plants? for some reason my wife has taken a great fancy to a large range of plants which all seem to have names beginning with “H” viz: Hosta, Heuchara, Heutunia, Heather, Heath, Hebe, Hydranga -you get the idea!!!

I do at the moment have absolutely no idea of how large a fuel tank I need. I would like a run time of 10 minutes so if I play with the figures -based on what I know of combustion I can perhaps get some approximation(?)

The perfect air to fuel ratio is 7:1 for Methanol...

I sent an enquiry e-mail to Model Technics to see which fuel they recommended and this is their reply:

Hi Ralph

I will answer your questions not in any particular order.

1  Todays engines run much better and more reliable with a small amount of nitromethane and 5% is not unreasonable.

2 All castor fuels in todays engines is not good. Tolerances and castor's nature to varnish causes problems in reliability, running etc due to the varnish build up. I would suggest therefore Sport 5 which has a small amount of castor as an additive. The rest of the oil being a highly regarded synthetic from Klotz.

Total oil content is 18%.

3  As for the acidity of the exhaust, well the exhaust is acidic due to the nature of the combustion process. The small amount of nitromethane will not increase the overall acidity of the exhaust as we have found in tests. So your wife’s roses and plants beginning with H are safe.

4 The main components of nitromethane combustion are members of the nitric acid family but nitrogen, water and  the oxides of carbon.

I hope this helps but if still unsure please phone.

So there we are. Any problems with a “Key Lime Pie” or “Obsidian” or “Creme  Freshe” variety of Heuchera is NOT MY FAULT!!!! The Hostas will still have to battle the slugs -but not the passing loco...

Now that the seasonal madness is in full swing I can divert my time into applied insanity(!) One  of the things that distinguishes this loco from all others is of course “The Fell System”. This is not only the infamous gearbox -but also the fact that the engines operated from a supercharged source of air. This was supplied by two “Rootes” style displacement compressors powered by two diesel engines running at constant speed. Thus the main power engines were fed a high degree of supercharge at low revs and this fell off at higher revs. To me it seems that I have to duplicate this in some manner. I do not have the technical ability or tools to produce a “Rootes” blower but I can produce fairly easily a centrifugal blower. There are two main methods of supercharging. Draw Through The Carb [DTTC] and compress the mixture in the supercharger, (the system used by Bentley). Or, Blow Through The Carb [BTTC] and modify the fuel system accordingly, (the system used by Mecedes-Benz). There are pluses and minuses to both systems. In the draw through you have a large volume of fuel and air churning and the heated output behaves more as a perfect gas than a fuel air mixture. In the blow through the hot compressed air is cooled by the evaporation of the fuel droplets inside the engine and there is less backfire risk. On the balance of ease I have selected the blow through the carb system. I have to design some method of pressurising the fuel tank other than by using the exhaust gasses from the silencer -as I doubt that they will have sufficient pressure to power the carb(?)

What I intend to use is technically speaking an axial flow compressor -or to be blunt a few computer cooling fans stacked together!!! I can stack three 25mm fans together to produce one fan. I don’t know how much “supercharging ” I will achieve -maybe a few millimetres of water. Each fan is rated at 155 Litres per minute, thus it should provide “supercharged air” for the engine up to 20,000 RPM -but as I said above the amount of supercharging may not be very high. However the simple fact that it IS running supercharged captures the spirit of the loco rather than being just a model of it!!!

On the second day of the New Year I was able to spend some time in my shed at last. Most of it was spent rebuilding the gearbox to a far stronger standard. I drilled down the grafted gear sides and united them with 2mm steel bolts. These were CA’ed into place along their length and then trimmed to size with a junior hacksaw. The bevel gears were introduced to my new(ish) Vee Blocks and I delicately and carefully drilled through the boss at the back with a 2mm drill and CA’ed a pin through it. I find that I have almost run out of 2mm roll pins -so I will have to use bolts only soon. The M4 steel washers that form the end loops for the “gear selectors” for the ballista were just as evil to fix as I imagined. I polished up everything nice and bright. As my former Brother in Law comments -”you have to be a SAINT to solder”, and applied the heat from my chefs torch. A little flux and then I hit it with the electrical solder, (good old Savbit). After some, “thinking about it”, it did bite into both the brass and the galvanised steel, then flow around the complete brass U section. The L brackets have been re-enforced with some offcuts of teak so the bevel shafts have something to rattle against.

The next thing to do is to investigate the final connection between the gearbox and the drive axles. In short -can we figure out how to assemble the last pieces of “chain” in situ???

The big 20 tooth sprocket that will take the drive from the gearbox above will have to be “custom cut” into the bogie as it is over 4cm wide. This means some “delicate” work with an angle grinder and a hacksaw to cut a slot for it to fit into. Looking at the sprocket again I think that I bite the bullet and wait until the budget can afford some 10 tooth sprockets and use them. This will mean an order for a further 6 of them from “Squires” -but that is not really a problem. The shopping list is starting to grow again!

Well the New Year has sprung and now two weeks into it I can return to work on my loco. After some self disgust I hacked away at the noses of the loco at each end -until I had something that looked “true”. The next stage was to apply basic auto repair systems!!! In short P40 then P38 and Squadron green putty... Now a couple of days after I began the “rhinoplasty” for the loco I am much happier how it looks. The problem was that the ABS sheet that I was using was too thin to take a true corner from. But if I made it thicker -then I could not bend it. Hacking away a section and then filling it in has provided a more smoother look to the nose. The shot below shows the result of wet sanding and filling. The section cut out can just be seen from the end of the side radiator to the windscreen, (as will be!)

See Picture 74.

Contrast the nice square to round shape with the raw shape found in Picture 71.

I am now busy starting to paint the things that I will not be able to paint once they are in position, and if they get scratched -then “tough”!!! The B0-B0 look of the loco means that it post 1954 -and it will be “Diesel Green”. What exactly this colour is -is debatable... But for the sake of accuracy, (meaning that the paint will be the same throughout my Green Diesels) -I declare this colour to be Rover Green 17. Since this is the colour that they use at Barrow Hill to paint the restored Deltics with -I have no quarms in cribbing it’s use.

The flycranks et al will have to be signal red. however I am going to depart from the accepted colour scheme for this and paint my wheels in light green with white rims. The orange stripe and the Lion will of course be there -but where I get my Lion from I am not yet sure(?)

Tomorrow I have to get my knees X-Rayed and I will grab this opportunity to visit my local model shop -it is just up from the DRI.  There I plan to raid the owners for information as to the price of Glow Fuel, and what they stock. I am still not sure if I require a fuel pump -or the exhaust pressure is going to be high enough to feed fuel to the carb(?)

I will admit to spending most of today simply looking at my model. This has nothing to do with personal vanity -but a lot to do with having to see whether I have the essential feel of the model... This normally involves looking at my drawings and then pasting / taping pieces of cutout to the model. Sometimes even when you have the piece in exactly the right position according to the drawing -you find a picture that contradicts it... Thus I admit I played shuffle board with my bits and pieces all over the roof of the model. The roof slots were made simply by sticking the lengths of ABS strip to the roof and then cutting through the now strengthened roof section with a cutting needle. The two central inspection hatches are one piece of ABS curved and then grooved -the two offset hatches are done in the same way. The doors and windows will have to be “black areas” as in order to cut these through I would have to cut through the main support brackets inside -this as they say is: “not a good idea!”

See Picture 75.

The one thing that I have to admit COMPLETE FAILURE with -is the twin exhaust system. I would dearly love to have the fumes from the glow engine expel from them. BUT the exhaust outlet from the silencer is in the wrong position and even if I used a length of silicone pipe to join it all up it would still not be “safe”. So, what I am going to do is to use a length of aluminium tube and vent the exhaust underneath the model. This will keep small fingers safe from hot exhaust gasses -but the ants and spiders might need to run rapidly(!)

The next thing to do is to make sure all the pieces that I have laboriously cobbled together actually interlock together. This may mean silver soldering more brackets to the gear box and then getting everything tapped and screwed to within an inch of its life -but with the G3 AGM at the end of next month I want to have something that can be seen to be a, “work in progress”, rather than a collection of modules...

Well today has been fairly productive(!) I have finished off building the radiator. This required cutting out a piece of poly carb, (always a messy job), and then clamping it onto the top of the radiator (XP1700 CPU heat sink as was...), and drilling down through the poly carb and ABS into the Aluminium below.

See Picture  76.


The holes in the heat sink were then drilled and tapped to M4. Some gasket paper and red gasket compound were suitably cut and smeared and the lot bolted together. The bolts were cropped to length once the compound had “set”.

See Picture 77.

Simple tests with a tap and a length of pipe have shown that although ugly -it is water tight.

The replacement PCB for my Milling machine arrived on Saturday and this morning was the first chance that I had to fit it. It was a Monday Morning and as usual things decided to “play up” after the weekend off... I fitted my PCB and -nothing happened. Basic tests with my “smiley” AVO showed things to be where they should be and I continuity in the right places dependant on the position of selector switches. Still it refused to go round.... I telephoned the Manufacturers -which being deaf is very hard work for me (!) and discovered that I had to short a link on the PCB to get it to function(?) After having unshipped and fitted the shorting link I applied power and both LEDS on the board lit up. Turning the pot knob and the motor growled, a little more and we had rotation!!!

Now that I have after 2 months plus of waiting a functioning Mill I can press ahead with things that have been waiting for it to work....

The first thing to do is to paint the wheels -this might sound a very strange thing to do but it does require a Mill to cut fly cranks etc with and once I have them I will not be able to paint the wheel spokes. A short squirt of spray primer and a some green paint from the pot and I have wheels for my loco.

The time is drawing near to start assembling my series of modules into a locomotive. I have ordered the bearing for the bogie wheels, the grub screws for the driver wheels and the bearing for the driver axles. The next thing on the shopping list was the 20 tooth gears for the drive axles and the additional “chain” for them. The body has had its first layer of grey primer and when this has hardened off (48 hours) then I will wet sand it flat and apply the next layer. Normally two layers is all that are required -then it is on with the green. I have to mark out and cut the windscreen holes in the front of the loco -this could be a rather delicate operation... Once the holes have been punched through they have to be “edged” and then the whole think primed again. Why did I not do this before the initial spraying? the reason is simple. The edges are very delicate and if I sprayed two coats of primer on then they would disappear under the layers.

A little further on in the week and  have progressed a bit more. The bearings for the front and rear bogies are now firmly installed and they scoot along the floor nicely. I decided to build a dedicated oil cooler for the torque convertor rather than having a cooling spiral in the water tank. This doubles the amount of cooling in the loco and lowers the strain on the water cooler. The oil cooler is made pretty much in the same manner as the water cooler except that I have used a heat sink from an Intel Pentium 2 series 3 cpu. This fits nicely across the front of the loco.

See Picture 78.
See Picture 79.

Well a busy and productive Saturday in the shed! Despite the finger numbing cold I did get some of the main targets that I wanted done. The first thing on the list was to drill and tap to M3. The next shot shows a driver wheel on the rotary table with a suitably modified centring peg!!!

See Picture 80.

The next task on the list was to chain drill the chassis to take the chains (!) Here is where my beautiful day hit  the skid pan... I had purchased from a TV Shopping Channel a set of Cryogenically hardened Cobolt Steel drills. The demonstration showed how they drilled the same drill to drill through glass, a file, and concrete plus they had a 10 year Warranty. I was sufficiently impressed to order a set there and then. They came the following Wednesday. I admit they looked very pretty and functionally rugged for the job. So, it was with high hopes I inserted the 3mm drill into my pillar drill and started to punch holes through the steel following the scored line.

See Picture 81.

On the third hole the drill broke....

See Picture 82.

If you look at the picture you can see where the hardened tip has simply come away from the drill proper. Needless to say “I was not impressed!!!!” I then fitted a standard TiN drill bit and continued to punch the rest of the holes. A slight attack with a hack saw and a set of mole grips and the resultant cactus edge is now visible. A quick once over with an angle grinder soon tidied it up.

See Picture 83.

It was now time to say “goodbye” to the M8 coach bolts that had provided the loco with axles for nearly four months now.  The axles I cut some 6mm bar into four 10 mm lengths squared them up on the lathe and then bored 3mm  diameter holes for 5mm into the ends of them .This will provide the holes to hold the lengths of M3 threaded bar that will hold the fly cranks to the ends of the axles.

See Picture 84.

The wheels will have aluminium tube shoes in them this will act as a crumple layer for the grub screws to bite into. The next step was to mangle the sprockets to fit the axles. The bore of the nylon sprockets is 4mm and they sit on a brass insert bush cast in. They had to go... I ripped out the bush on the lathe with a 6mm drill.

See Picture 85.

I now had to make a new bush for fixing for the sprocket. A length of Aluminium rod provided the new bushing. Oh so slowly I drilled down the length of the rod and out the other side. I was lucky if I could cut 3mm down it before the bit clogged up and I seemed to spend HOURS simply winding the bit in and out of the hole to brush the swarf off the end.

See Picture 86.

Once I had my “tube” I then clamped it up and drilled the 3mm holes down its length giving me what my son called a “small flute”.

See Picture 87.

I put it back into the lathe and used the parting tool to cut myself some slices from the tube. Bolting the slice to a sprocket and then drilling 2.5mm holes in the two provides union. There was a slight panic stricken moment when I had to count up to see if I actually HAD enough 2.5mm nuts and bolts to complete this. The double sprockets have been fitted with three 2.5mm nuts and bolts as these will have to take rather more strain that then the end ones.

See Picture 88.

The following shot shows the double sprocket and the single sprocket (unfortunately still on M6 coach bolts....) When it comes to actually fitting the sprockets I intend to drill down the already present 3mm holes and through the steel axle shaft and then pin the lot together.

See Picture 89.

The outer of the two sprockets connect to the gearbox above. In the original this would have been done via; an idler gear, to a quill drive, to the driven axles -but to be honest given the reduction and the torque convertor I do not think that this particular loco will need one as it will have no “cold snatch” from electric motors.  The next stage of operations will be to section and slot the power bogies to take the modified sprockets. The chain return between them is very likely going to have to sit in an external “conduit” to keep it clear of muck and leaves etc.

See Picture 90.

After a respite to deal with a slight case of flu!!! The chains have been assembled and the fore and aft chains fitted to the output sprockets. The single sprocket is the outer and the double sprocket the inner set. The transmission between the inner and outer axles will be via conrods and the link between the two bogies via the chains. This is because chain systems only work by pulling -and it gives a flexibility not found in a rigid system. Chains react differently depending on which direction they are tensioned thus the requirement for chain tensioners to keep the forces equal regardless of rotation. I will have to screw together some form of “slipper” tensioner as there isn’t enough room to produce a tensioning sprocket.

However initial tests with a wheel brace connected to the “input” shaft of the gear box show that it will propel the loco forwards -but without the tensioners the “take up” of the chains is very slow.

The postman has been busy and now have a fuel tank for my loco along with a mounting bracket (nylon) for my engine with, (at the insistence of my wife), a nice bright shiny purple anodised fuel filter. I was simply going to buy a plain aluminium one -but she liked the colour.... I did however sneak in the plain grey plastic exhaust tubing -despite all the “nice colours” that were on offer(!) The plastic plumbing tubing is clear -the fluids that will flow through them will be colourful enough...

The outer shell has finally been given it coat of green paint. This went better than I thought it would as well the loco has a very “sad” expression on its face -I cannot explain it any other way. After two coats of high build primer some soap and wet sanding I had a surface that was “flat” and all the runs and sags had been rubbed down. The sun duly came out and the wind dropped. After some applied “rattling” I sprayed the body with BL Rover Green 17 and I was initially horrified!!! It was FAR too light... After a deep heavy sigh I put it back in the shed to set overnight. I put a “post it” on the fridge which read “buy paint stripper” The nighttime worked some kind of magic as the morning brought a shell the was dark glossy green and almost a perfect match for the colour I wanted it to be. The body now needs its roof coating with “Dark Grey”.

See Picture 91.

After a not so brief spell digging holes in my garden (more next week...) I have some time again to play with my loco -yes it is throwing it down again! I ordered some more bits from Technobots -these are the 16 tooth sprockets that I will mangle to produce the flycranks and the aluminium pulleys that will connect the engine to the torque convertor and the torque convertor to the gear box. Why Pulleys? These have self damping connections -in short big rubber bands. This will enable me to have a flexible connection between the engine and the torque convertor, direct alignment will not be required -it makes it simpler and if all else fails it is a easily removable module.

See PIcture 92.

In the shot above you can see the main pulley on the engine -which will have the rubber band to the pulley on the torque convertor. The pencil line to the left of it shows the centre line of the torque convertor. On the left of the line is the linear actuator that will be used to change gears.

The nice people at “Just Engines” who supplied me with the ASP 46M engine also supplied me with the fuel, water and oil tanks. You may remember that I was looking for something to cobble up a water and oil tank system from, well I had to mangle part of their “economy” range of fuel tanks and I have something that not only looks as if was designed to fit there -it should work too. The system has two L shaped pipes -one of which has suffered at my hands and is now the “return” to the tank. The feed still has it’s “clunk” at the end of it. The fuel tank is as supplied at 8oz and the water / oil tanks are 20oz. The dimensions for these are given in imperial and I had to beg an imperial ruler from my wife, (Quilting is still quite firmly Imperial!!!)

See Picture 93.

Yes, I know it looks messy in the photo -but it will look a lot neater once the cradles are wired in. The “returns’ are clearly visible as are the air vent pipes inside the tanks. However they fit nicely when taped into position and the next instalment for the loco awaits -the pumps.

After much thought I decided to use Lucas style windscreen washer pumps and then mangle them for my purpose. They are cheap, (reasonably reliable), and very common. I will have to remove the casing, (delicate work with a hacksaw...), and then extract the vitals.

Well another wet weekend (and it is now snowing...) However on the plus side the pumps have arrived from the Channel Isles and I have been playing with them. The rate of flow was the first thing I had to find out. So, after duly filling a large milk bottle (3 Llitres ) I connected the pump up and times how long it took to pump out 1 litre. The answer was 48 Seconds. This gives me a flow rate of 1.25 litres per minute. The tanks on the loco are 634 cm3 thus the entire contents of the tank is pumped twice per minute. Don't you just love easy maths!!! The next experiment was rather more messy -as I had to find out at what "pressure" my pump was delivering its liquid. This was found by simply lifting the out let pipe until no more water flowed out of it -the slightly soggy answer was 2.35 metres. Translating this it becomes 0.21 BAR of pressure. Once the primary experiments were out of the way it was time to cut open the pump....

There is a suitable gap between the motor and the plastic wall of the pump body. It should be possible to cut some vent holes to help cool the motor as it will be running throughout the progress of the loco.

The next thing on the shopping list are some solder on "nipples" for all the 1/8th inch plumbing -these will probably come from MaccModels. The pressure from the pump is enough to force the connections from the rubber pipe -and yes it was very funny!!!

I now have the 3mm bearings for the conrods and the brass strip that will form them. The next step will be to produce the flycranks from the sprokets. This is done by sawing off a section of the sprocket and then grinding off the teeth of the sproket. I know this sounds very wasteful -but it is guarenteed to work. The centre of the, (now), flycrank is epoxied to the 3mm threaded insert and nutted up. This not only holds it while it sets -but gives more mechanical "grip" to the flycrank. A little dressing up with a few suitable sections of ABS scrap and I have something that not only looks like -but actually will -work!

As with the "Krokodil" the main problem will be getting the flycranks all synchronised with the rotation. The original had two huge long ones, then split into 4 shorter ones -due to resonances at high speed. I wonder if I should bite the bullet and produce a "4 Quarters" layout in which non of the conrods are in alignment and they occupy the 90 degree sections of the circle. I know that I have phrased this VERY badly but let me see if I can explain it better(?)

front lhs at 00 degrees.
front rhs at 90 degrees.
rear lhs at 180 degrees.
rear rhs at 270 degrees.

This SHOULD even out the vibrational modes of the system and hopefully give me a smoother running loco.

This weekend (26th of Feb 2011) is the Gauge '3' AGM. I have been busy building a trainsporter. I intend to get the Fell and the Krokodil to Biggleswade and back... Maplins supplied the foldable trolley and my son supplied -his toy box!. I looked at it and then dropped the Fell chassis in it -it fit exactly. I them dropped the Krokodil body into the box -that fitted it exactly too. Never in a million years would I have expected this to happen and I confess that I did laugh for a few minutes at the irony of it. If all else fails we will have a seat on the train -by sitting on the trains...

Well nearly one week after the AGM -how did it go? I have to say that the AGM itself went very well indeed and I could have spent rather more than I did at the traders.... Fortunately I ran out of money and non of them would take "plastic" -otherwise I would have been in hock for many a month!!! I did come home with 8 sets of Carriage wheels -which will go with my 4 bogie sets and slowly the bits for a carriage amass -more later! Getting to Biggleswade was nasty -there is no other word for it. Since my son wanted to do some "trainspotting" I studied the time tables and worked out my route. If it was not subject to any delays it would be an easy run. We got up at 3:30 am had a decent "college" breakfast and made our way to Derby Midland station for the 6:01 train to London. We got on board the "Meridian" which then only paused at Leicester before hammering it to St Pancras International -total time on train 93 minutes and the coffee shops were open for more food for son (and an espresso  or three for daddy!). He got to see Javelins and Eurostars and more Meridians. Even though it has been several years -I still expect to see the "Gasometers" on the final approach to St Pancras...

We then dragged the box across the road to Kings Cross -were things began to fall apart -big time. I did not know that "Kings" was being "restored" and that also -nothing worked. The only functioning display board we could find was on the end of Platform 8. When I say functioning  I mean that it was lit up -but that was all. When this photo was taken the time was 8:09. The roof leaked and (of course) it was raining.

See Picture 94.

I wasn't until 8:18 am that we knew which platform the train was going to arrive at. However what we did not know -was how to get from Platform 8 to Platform 6. Fortunately a Porter gave a lift on a towed "Brute" trolley and we made it just before the doors closed.

We got to the AGM despite the map and unpacked. In case you are wondering I do build large locomotives -even for Gauge '3'. Here is a shot of the Fell with my sons loco the (as yet) unfinished LMS 1831 with a GWR Pannier tank for comparison

See Picture 95.

We left the AGM shortly after 1:30 pm and got home for just before 6:20 pm. I managed to eat some Chinese from the takeaway and my son promptly fell asleep after having munched his bag of chips and he was out until 10:00 am the next day. I got him and my wife upstairs and then shortly after 8:30mpm looked at my wife and kissed her -and then somehow it was 8:30 am Sunday!!!

In short we had a great day out.

A couple of weeks have passed since the AGM and yesterday was St Patricks day. So what have I been doing in the meantime -the answer is getting very wet! The only real way to find out if my design for a torque convertor works well is to make a plastic sheet model and wind it up to speed. My test fluid was tap water and my test plates made of ABS sheet. Now there is a function of propellor design called "rooster tailing" in which the waste energy of the propellor flings up a stream of water in the familar "rooster tail" of racing hydroplanes. So the amount of water that my driver disc converts to a rooster tail shows the direct efficiency of my design. In short I produced some magnificent rooster tails until I got the shape that I needed.

In the original design I had nice evenly spaced holes, this did S@D all.
I then tried slots. Better.
I then tried a series of small holes working out in a spiral, it took me a day and half to produce, and did S@D all.
By mistake I drilled a hole that was obviously too close to the centre shaft (groaned) and completed the series. This worked perfectly...

SO I have to have the holes for the discs close to the centre. At the moment the only reason I can think of is that the centre is rotating slower thus fluid has more time to penetrate the cavity and thus create more friction between the plates(?)

What follows is a true rendition of my pet term "Kitchen Sink Engineering"... This shows the test rig for my evaluation (!) Yes I know it is really "Heath Robinson" but the fact is that it does exactly what it says on the tin -or in this case -the Muller Rice pot! The length of 4mm shaft is held in place with a couple of notches sawn into the side and some CA. The driver plate is driven by a power screwdriver separarted from the driven by a spacer washer and the fluid is -used  cooking oil!!!

See Picture 96.

The next shot shows the driver plate being spun by the screwdriver and the fluid forming the small rooster tail around the driven plate and transferring the energy to the driven plate and it spins with it. When the screwdriver stops then the oil drains out from between the plates. I now understand perfectly why there was a STEP UP gear to the main convertor on the Voith system. As you can see by the errm "excess oil" splatted around. The system works far better at higher revs. The main problem being that oil is now centrifuged off the plates -and of course goes everywhere....

The plates are made from the resident powder cast gears -it is nice to see them actually at work rather than sitting in the bottom of the draw.

See Picture 97.

I looked and thought -and looked and thought -and changed my mind!!! Although I still like the idea of the Tesla disc system I deciede to go with a paddle wheel design instead. Most of the mayths that I didi for the tesla design still hold true for the paddle wheel . So, after a good cup of strong tea I set down in my shed and began the days labors.

The first thing to do was to fix the driven plate to the shaft. Out with the carbon arc torch and dial 40 Amps on the welding plant a couple of dabs with the stick of SIFbronze and the job was done.

See Picture 98.

The next step was to similarly braze the output shaft to its gear wheel.

See Picture 99.

The next question was how to fix the paddles to the plates? This was simply done by using the rotary table and drilling a series of 2mm holes around the edge. Some CA to fix the paddles (actually 2cm lengths of brass U section), to the plates and drill through them. The nuts and bolts then held everything in position until I was ready to hit it with the MAPP gas and the silver solder. By brazing the shafts before hand I was sure that I would not disturb the joint!

See Picture 100 (!)

The main shaft is held in a simple plate U frame with the driven plate free to rotate on the same shaft. The output shaft is held by a scrap piece of box section and this meshes with the central gear on the driven plate.

The next twp shots show the assembled torque convertor.

See Picture 101.
See Picture 102.

The next problem is going to be a suitable oil leak proof cladding for all this to go around in...

I know it has been  couple of weeks since I last put anything on this -but I assure you I have been busy! Now that the torque convertor is finished -but still not "clad" I have been surveying the market for what  need to start it. I bought myself a rechargable glow clip and a glow plug spanner. The latter has useful nut sizes on it and it may get pressed into service for other duties.

See Picture 103.

The next item in the shopping cart was a starter motor. I originally designed the front oil cooler to swing out of the way to get the starter motor to nose up to the front of the engine, and this it does very well.

See Picture 104.


The problem is not one that I could have foreseen though.... The problem is that my hands are really too big to fit comfortably in the "grip space" of the starter. The starter has an oval push pad to connect it to the battery pack and I can press this with three of my fingers. The little finger I have to hold stiffly out -emulating a famous species of "Invader"!!!

See Picture 105.

The other thing that really should have occured to me is that it has to held in my left hand leaving my right hand to do the business with the glow clip. This would not normally be a problem for 90% of the population -however for the 10% of us of the Sinister persuasion -doing things with the  right hand is just awful!!! YES I admit it, I own a pen with a bent nib for writing left to right.

Another sunny afternoon spent in the safety of my shed! The problem with the too small grip aperture has been solved with the aid of a saw and some "polymorph" which is a resin that is squishy when hot and rigid when cold -it is also reusable. I now have a perfectly formed custom grip for my starter motor -no more "stiff little fingered aliens" around here! The testing of the starter motor to the engine has proved that I need what is called a "cascade" battery supply. This is a set of batteries in parallel to produce a very high impulse current. The eventual system will use six 6 volt SLAs to produce three 12 volt batteries in parallel. This will give me a cranking supply of 13.5Ah at 12 volts. The peak load from each chain is not really that high but the sum of them is "enough" to turn the engine over at more than idle speed I think(?)

Now that things are begining to form in the aether I can spend some time on the wiring for my loco. There has to be two independant supplies -one permanantly supplying power to the fans and the  pumps -the other supplying power to the RX and the servos. The next problem on the list is laughable!!! The amount of force that I need to press the rubber insert against the coned flywheel of the engine -causes the engine to move backwards on its mounting brackets. I have a friend coming who will advise me on a suitable system to use -he will probably weld the brackets up for me too!

Well the "consultation" went well and I have a good idea of how to rebuild my support brackets for my engine. Once they have been brazed together it would take an elephant to move it!!! I have spent most of this afternoon playing with my coolant system. I knew that the system had never been played with "in anger" and it was time to see if it functioned correctly. The first thing I had to do was to find and fix the leaks! These were due to things "settling in" as the sealant moved during the stresses of heating (and tighten the odd nut or two). I also had to wire the ends of the piping as once the seals were functioning they were the next thing that could (and did) move! In order to check wether my seals were working I mixed blue food colouring with the water. Since the system only functions when it is full of water the only method of priming it is to suck hard on one end of the plumbing... YES I have severe "blue tongue plague". The pump gets a little warm when running -but I think it is within parameters -I might drill a few coolant holes in the side of the plastic casing to let a little air through it?

The pump draws 2.5 Amperes when in full thrust thus the two pumps will draw 5 Amperes when the system is running and the loco is in motion. I plan for a running time of 10 minutes -but this is dependant on the consumption of fuel -the fuel tank is 225ml or 8 Fluid ozs. I picked up my 1 litre bottle of glow fuel and "After-Run-Oil" from the local model shop. The oil content is slightly low at 16%, (ASP's like 18%), and the NitroMethane more than a little high at 20%, (it is "timed" at 5%) -but it is the only one I have so it will "do" for initial testing.
 
A sunny Sunday afternoon spent safely in the kitchen and shed. I fabricated the new mounts for the engine -they are of 3mm thick steel and use a steel re-enforcing bracket to hold it "true". I have bolted it through the chassis members with 5mm bolts -it is not going to move again! Now that the position of the engine ifixed in 3 space I can get around to connecting the propshaft from the torque convertor to the gearbox. This runs underneath the engine and through a slot in the engine mount. There were some very worrying moments as I twirled the propshaft and there were loud "bangs" as the bevel gears jumped on their axles. The reason turned out to be quite simple -but fatal for the insect involved -some delicate brushing away of pieces of corpse then re-oiling and the gearbox whired away niceley

This shot shows the new engine mount.

See Picture 106.

The next shot shows the test assembly of the torque convertor and its propshaft. The belt takeoff from the engine to the input pulley of the convertor and the output pulley of the convertor to the propshaft. The propshaft will sit between two sets of ball races in the position of the brackets. The brass union for the propshaft and the input shaft to the gearbox can be seen directly underneath the engine carburettor.

See Picture 107.


Today was the May Day Bank Holiday -so I spent it in my shed! I had specified to the rest of the household that this was a "shed day" so they ate their sandwiches for lunch in quiet meditation. The first operation fo the day was to build the "cranking handle" for the engine. When the torque convertor etc are positioned there will not be enough room for the staret motor to get into position -hence some form of reach rod was required. I made this from 10mm silver steel bar -a little overkill -but it was handy. The end I drilled out to 3,5mm on the lathe and then tapped it to M4 on the lathe. This is the first time I have done it this way and it was slightly scary the way the tap was "eaten" by the steel bar. A length of M4 threaded rod was fitted and then the free propellor shaft fitting that came with the engine was added.

See Picture 108.

The next thing was to hit it with the silver solder and unify all the parts. This is somewhat ugly looking result. The yellow colour comes from the Zinc plating on the propellor shaft fitting. If you are welding then galvanised stuff is a definate NO -NO! but with soldering -it actually makes life easier.

See Picture 109.

I now come to the proudest part of the creation!!! The 10mm steel bar is then punch fitted to a Hose Lock fitting and then a 3mm nut and bolt pinned the two together. The hose fitting meshes perfectly with the yellow silicone cup on the starter.

See Picture 110.

Lunchtime and sandwiches saw the living room converted to my drafting room. The next shot shows the designs for the torque convertor housing. I settled on one using an asymetric roof -because it made life easier to build. As you can see one side of it has a radius of 4cm and the other 3cm.

See Picture 111.

Back in the shed I began to cut up the highly unwilling paxolin sheet into the correct shape. The sawing of the straight sides was the hard part the curves I simply ground out on the grindstone. OK it smelt a bit -but it was quick! The ends are made from two pieces of paxolin that wrap around the holes an then lock together. There is a 3mm nut and bolt locking them to the uprights on the torque convertor.

See Picture 112.

The internal space of the torque convertor is going to be filled with shaped pieces of balsa wood. Once I seal everything with epoxy the substance that I used to make the shape will not matter -but the shape will...

See Picture 113.

Saturday is scheduled to be "Fell Fire Day"(!) The coolant system has been bled to within an inch of its life and the radiator fan has been whirring away like a top. All the power bricks (SLAs) have been charged and everything awaits the dawn of what promises to be a very noisy day.... I have been asked by a few people to take a "video" of the device in action. Well as a far as possible I will try to -but we might be a little busy!!!

Well -I got it to fire... Now it seems that I have to re-tighten every single nut and bolt on the loco!!! The model is covered with oil -most of it from the self undoing allen bolts on the exhaust manifold. A good friend who was there to "hold my hand" commented "Is this what is meant by self lubricating???" At the end of the first 2 minute test run due to vibration I had "lost" 1 M4 nut and bolt and several M3 ones -these were nicely rolling around on the sheet of ply on the workmate . Unfortunately these were the ones holding the engine to the bracket... The good news is that the coolant system performed well, but then on the second test run -it blew up!!! The fan died on me and with the coolant temperature rapidly rising I put my thumb over the carb intake and everything stopped. The temperature of the coolant rose and held steady at 30C during the first test and the air temperature was a warm 23C. As per the instructions we allowed the engine to cool -this allowed us time to retighten all the loosened nuts. The engine had initially started with "some words" but it started cleanly the second time. I will have to modify my starter system though, the yellow rubber cup tends to fly off when I pull the starter away from the running engine. I think that I also need to investigate some form of "over run" clutch for it(?)

The next thing on the shopping list is a shed load of lock nuts and a large tube of thread lock!!!

The fuel clips didn't work to my satisfaction and weeped, so I undid them and WIRED the hoses to the pipes -this held it all leak proof. I also need to find some method of easily filling the fuel tank when it is locked into position. At the moment I am using a 6oz "squirty bottle" with a valve and filling the tank that way. The engine does seem to like guzzling fuel though -so perhaps at some later date I will investigate converting it to petrol? The people that I bought the engine from do a petrol conversion kit complete with "timing disc". This may be something to think about as it would ease the types of fuel that I would have to store -at the moment there is 2-stroke for the rotavator, 4 star for the lawnmower and the glow fuel -not to add the gallons of parafin for the greenhouse heaters.

The noise was as bad as everyone feared. I was the only one NOT wearing ear defenders, and this was with the "Super Quiet" silencer...

I think that I terrified the neighbours though! A voice calls out "The System is LIVE", there is a muted whirring from the pumps, then "Cranking!", the starter screams and then the engine squeals away at 1/4 throttle. The longest I have had it running is for 6 minutes on the second run, I have yet to follow through with the instructions to run the engine at full trottle for 12 minutes. The crib sheet says that "run in" will take around 30 to 60 minutes -now everything will have to wait for a new fan and some lock nuts/thread lock to come through the post.

Am I unhappy -NO. It was a test run and as such it provides data on the problems to be solved.

When I am ready to test things again I will have to do a time temperature and voltage chart. This will give me some idea as to the peak temperatures from the cooling system and the drain on the batteries as time progresses. I will have redically re-design some of the plumbing as the only way I could drain the fuel from the tank was to blow down the silicone tube connected to the exhaust silencer and then draining via siphon the fuel from the tank out of the feed pipe to the carb. Similarly fueling the loco will have to be arranged, the squeezy bottle works -but it obviously a short term solution to the problem.

Well the fan has arrived and it seems pretty potent at 39CFM and it slotted into the hole perfectly. I did some experiments to see if "blowing" was better than "sucking" air through the radiator gills and although there was no detectable difference in the amount of heat that was extracted -I was told by "Her  Pinkness" that blowing was quieter -so this is the way it will operate.

The rest of the stuff arrived this morning, (fortunately the weather was with me) -and it threw it down all day!!! I started out by replacing all the nuts with nylock nuts these should discourage the bolts from moving (hopefully!). The torque convertor was the next victim on the list and I mixed up some epoxy to try and seal all the edges of the t/c, once that had set I then daubed P40 over all the places that looked as if there was light coming through them, (and with what ever was left I simply splatted on too...) It looks somewhat "hairy" with all the loose strands sticking out of the resin but this is a minor point. I got the rubber drive bands and fitted them. This means that there is (in theory) just the one connection to go between the engine and the gearbox -the fluid! The next shot shows the days progress.

See Picture 114.

Famous Last Words...

The day dawned black wet and windy. Perfect weather for an excuse to go and play in the shed with. I had been experimenting with my pump for the torque convertor and had got it to work both forwards (flood) and reverse (bail) quite naicely with the oil mix that I was going to use. The only problem is that with the viscosity of the oil the pump will not "self prime" as it would with water -so there is going to have to be some form of detcor to say when the T/C is nearly empty. The pump is of the gear displacement type and once the oil has reached the gears it squirts it quite effectively.

See Picture 115.


K&S provided the brass sheet that was to produce the wrapper for the T/C and some slight persuasion with the slips formed the correct curve. This was duly edged with some brass L section and this soldered onto the curved sheet.

See Picture 116.

The wrapper was then wrapped around the body of the T/C and secred with a handy vise while thegasket and screws were fitted over the next two hours...

See Picture 117.

Nedless to say several "words" were uttered whilst trying to fit the wrapper and the new scars from the raw edges dripped nicely(!)

The "pressure test" as such consisted of a length of pipe connected to the T/C and it filled with oil and it withstood 1 metre pressure of oil -this being the longest length ofsuitable pipe that I had. The fiiled T/C was then connected to the chuck of the lathe via long rubber band and it twirled nicely at both ends. Everything was set for "GO!"

I drained the T/C fitted, it into position ,"dodged" the flying yellow rubber cup thing (I really must do something about that!) and the engine fired. Nothing seemed untoward so I hit the switch to "flood" position -the cable to the T/C pump was 2 metres long and I was standing behind the corner! There are some sounds that stick in your memory -before I lost my hearing there was one sound that was as unique as it was lethal. This was the sound of "Disc Dive Motor Head Bump" which is the sound of a set of read heads on a disc platter bouncing from top to bottom and knocking chunks off of the surface. I could describe it as the sound of someone feeding a musical  box mechanism into a meat grinder.

IT was THAT sort of sound.

The engine stopped.

I peeked around the corner and there was nothing visibly wrong -there was a gap where the T/C should be and it was visible on the floor beside the loco.  The rubber band was "somewhere" and oil was EVERYWHERE!!!

I initially though that one of the driven plate turbine blades had come off -but after examining the debris showed that all of my turbine blades were still firmly fixed to the plate. What had happened was as the oil filled the T/C the turbine blades hit the oil and the shock of the impact snapped pieces off of them. I had a good cry in my beer and did the only thing possible -I went on the Internet and I asked for help!!! 

Help arrived by 9pm the same day. The problem IS a type of Oleo Kinetic Shock -but the shock is due to the foaming of the oil. In short CAVITATION. The method advised by "The Person from Glasgow" is to use a modern synthetic and to feed the oil from the centre outwards. This spins the oil up to speed as it fills the T/C. Draining it will involve some valve and plumbing work. He is also going to provide some "suitable alloy" to make the turbines from. Yes -the nymphomaniac metal... I have never tried to work with it  but I am told that it is "interesting" to say the least.

I have been drafting some designes for the new T/C and I am pleased to say that there are very few pieces of waste paper bin fodder so far. Now that I have nothing to do whilst I sit and design things I have turned my attention to the exhaust system.  This is a "Super Quiet" silencer supplied by the nice people at Just Engines who also supplied the engine.  They do give some help in altering it to be quieter on their web site and I e-mailed them to check out an idea that I was looking at.



The "Super Quiet" is made in three sections, it is held together by one huge long bolt  and the end of part 3 is THREADED -the lock nut at the end simply stops anything unwinding. It has one baffle plate of six holes with vanes and is located in position "B". They do suggest moving it to position "A" and you can experiment with flattening the vanes. Another suggestion they give is to partially obstruct the exhast vent in Part 3 with an M4 bolt. What I have done is to manufacture a second baffle plate (in short a simple piece of brass sheet with seven 4mm holes!) Located this in position "B" alongside the supplied plate in position "A" and also fitted a section of M4 threaded bolt through the exhaust vent. This will no doubt RUIN the "top end" of the engine but since it is never likely to hit that in it life I feel quite confident that all will be well.

Well at the end of the second afternoon of test running I am happy to say that the engine was "noticably" quieter. It still sprayed oil over everything but I did not lose too many nuts and bolts this time -but I did lose some from different places this time... This series of tests was designed to examine how well my cooling system was now running so -for the first time we had an "endurence" test. The first run was two minutes long and the initial readings from startup were:

1: 24 C
2: 27 C

After a pause to tighten up the ehaust system and see where all the new nuts and bolts had come from... I gave up on using a gasket for the engine to exhaust system, (bits of it were just splattered around anyway! ) and simply applied jointing compound to the two cleaned faces and tightened everything up solid. This seems to be the best method as they were still tight at the end of the second run.

1: 32 C
2: 34 C
3: 36 C
4: 36 C
5: 36 C
6: 36 C

So, looking at the results it appears that my cooling system can keep the motor at a constant temperature of 36 C. This gives me something to work on. I now have a steady state temperature of 36 C and a rate of flow which is 1.2 litres per minute. This means that the radiator is cooling the volume of liquid over it at the same rate regardless of the volume -in short this means that I can reduce the volume of the tank. In theory I could dispense with the tank -but perhaps not yet!!!

Tomorrow (Saturday) is scheduled for another test run. I have been busy unscrewing and dabbing "blue threadlok" and "stiffnuts" over and in any threaded item that I can get at! The aim of this series of tests is to see just how low a rev rate I can get on my engine and (possibly more importantly) how lean a mixture I can get it to run on. I do expect to have to play "start rich" and "run lean" games for some time. I have put the air filter on the engine for the first time. I confess that it does look somewhat comical like a large yellow clowns nose perched on the end of its rubber elbow. The reason for fitting it at this time was that beforehand I could look down the venturi and gauge (roughly) at what point I was at -min to full throttle. Now the aim is to set the throttle arm and leave it. The restriction through the air filter will alter the mixture to be richer in any case.

For those interested in more information on the loco there has just been published June 2011 a 4 page article in the magazine "Traction" which you might find useful. Previously to this I only knew of an article in the magazine "Back Tracks" from Feb 2009 -which is more detailed and goes into the design and technical aspects of it more.

When I began my thread on "The Gauge '3' Society Forum" I used the old schoolgirl skipping chant by way of introduction:

"I do not like thee Dr Fell,
The reason why -I cannot tell,
The only thing I know (and know full well),
I do not like thee Dr Fell."

The article in "Traction" begins with the same refrain... (And I thought I was being so original!!!)

Looking at the pools of oil left after each series of test runs -annoys me. There will have to be some form of "scrubber" on the exhaust stack -or at the very least a drip tray... This does raise the question -what do I do with all this oil? I am not au fait with Klotz -but it does seem to be a very good lubricant even when it has been through the engine. This does raise the problem of oily rails so it does seem to be "needful thing" that we have to contain the spent oil, (somehow).

Well possibly the worst series of stupid problems in the world happened...

It began with the starter rod pin shearing.
Then the flywheel nut unscrewed.
Then the drive pulley on the starter motor unscrewed.
And then to cap it all -the drive belt fouled the motor and had to be cut to pieces ....

I looked at Martyn, he looked at me and we both said; "Enough -lets go make tea".

So we did.

After having had a good cup of tea and several days having passed I have decided to abandon the starter system that I am currently using. What the new starter system will be is as follows, and to be honest it is a genuine cobbled together mish mash. I saw off the prop shaft adaptor on the starter rod. I then bore out a 14mm 1/4 inch drive socket to a bore of 10mm and I braze it to the starter rod. This gives me a rigid fixed connection. To the other end (sawn off) I fit a "one way bearing"  as it is now called, but I still want to call it an "over run clutch" -with an 8mm bore. This then provides a secure fitting to the driven end of the engine. Once the engine fires the over run clutch dis-engages and the starter motor can be switched off with the engine still running then (hopefully) the 14mm socket uncouples from the M14 nut without it flying off -somewhere!

The parts are on order and I await them in the post.

Tuesday morning the parts arrived in the post. I now have a nice satin finish Chrome Vanadium 14mm socket and a 14mm hex nut "one way bearing" for it to connect to. I hunted around the scraps draws in the shed and extracted a length of 8mm rod, filed the ends smooth(ish) and slipped on the bearing. As promised the bearing went around only one way. So far so good -I thought. I drilled a 3mm hole through the end of the rod and affixed it in the spade jaws of the engine and nutted it up. I tried to turn the engine via the bearing -and the nut  came away in my fingers... Needless to say -I was not best pleased!!! The nut is at best a friction fit to the bearing and it could have just not seated before it was engaged to the bearing. I whipped out the CA and now it is VERY firmly fixed to the hex nut....

The next shot shows the hex bearing sitting on the length of 8mm rod.

See Picture 119.

Having looked at the 14mm socket I am wondering if I could simply cheat and drive it from my battery drill/driver. The thing does have enough torque to turn over the engine and it is a lot simpler than all the faffing around with milling and brazing -plus at the end of it I have a 14mm socket that I can use elsewhere. Hmmmm....

See Picture 120.

Having slept on the subject I decided that as the socket was only £2.54p I could afford to buy another one -if I needed one. So, the socket went to the lathe and then the fun and games began. The first thing I tried was a 10mm TC end mill this cut a nice groove through the curved edge of the socket hole and then stopped... the next thing I tried was a 10mm Cobolt drill. This cut a nice conical shape into the socket -and then stopped... Hmmm... I seemed to be able to get a nice cut  with the edges of the cutter and then as the amount of cutting surface increased the amount of pressure that I could get on the cutting edge I hit a point of no return -in which the amount of force I could apply with the screws was not enough to make the cutter bite into the metal. I unlimbered my "ultimate weapon" as regards holes.

I fitted an 8mm boring bar to my head and slowly opened it out a few millos at a time. After the course of an hour I had removed enough Chrome Vanadium steel to be able to get the entire cutter width of the boring bar into the hole. NOW things began to move!!! Now you will have noticed that using an 8mm boring bar in a 10mm hole is "a bit tight" as they say -and I will be the first to admit tht the head did bung up with chippings and stall the lathe on far too many occassions.

See Picture 121.

After some polishing at very high speed I POURED Superglue into the gap and left it in the jaws of the lathe to set over an hour or so -time for lunch(!)

See Picture 122.

The next shot shows the completed starter socket and the lathed to size stub end of the over run clutch fitted to the "business end" of the engine.

See Picture 123.

So -what has been happening in the the weeks since the last entry to this? Well actually quite a lot -but very little to report on. The starter system works and the engine has done endurence runs of 20 minutes. The peak temperature reached by the coolant was 43C with an ambient air temp of 23C at that time. The superglue did eventually give way and I was forced to do something that I really should have done on the first day -BRAZE the two parts together. The engine is now well "run in" and I have been able to reduce the mixture down to something that is both livable with and runable with! During the running in process I was using a mixture so rich that it gulped down 250ml of fuel in 5 minutes.

Now that the engine side of the system seems to be ok and is "a known unknown" I can get down to the business of building a torque convertor. Rather than oil I have decided to use water. There are two reasons for this -the stuff is cheap and easy to get hold of... I did "jig" my torque convertor for SAE 30 oil -but this is in short supply so Aqua Impura is what I am going to use. Since I am using water I can simply use two propellers back to back -non of this tedious mucking about with discs and moduli of fluid surface tension. The simple fact is that I was too ambitious and should have gone for the simple option straight off -there learn from my mistakes!!! I ordered two nice brass props from an internet supplier who promptly told me they were out of stock and I would have to wait two weeks for them to be shipped (ha!) from Holland. I then got two props from the suppliers but with the wrong thread size. Needless to say this did not make me happy and the sales person on the other end of the line was made very aware of the fact. They did offer to replace them if I sent them back and they would order another pair from Holland and I could have them in another two weeks. (I told them, "No thank you" -even if I did not use quite those words...)

One of the props will have to be bored to 5mm to take the input shaft. The other will have to be bored to 6mm and then a "blind" hole of 10mm cut in the front of the prop with an end mill for the ball race to fit into. This "locks" the driven prop directly in line with the driver prop from the engine. There will have to be some return plumbing in the cavity to allow the water to circulate around the props. Another advantage is that being water the props are designed to cope with a low level of water as they are lowered into the water. Thus there "should" be no problems with cavitation. The top speed of the props is 4,500 RPM and I "think" that I have the engine running at below that.

So, nearly six weeks from the last real session on model building -what have I been doing on this loco. The sad fact is not a lot -but we do have a nice new kitchen, a new back door and ground floor "facilities"...

Now that it is safe to begin work in the kitchen again(!)

This details the production of Torque Convertor mark 3.

Having aquired two propellors  (see above) I then began to mangle them to requirements. The first prop was brored out to 5mm and a 5mm bolt soft soldered to it. The bolt them went into the lathe, centre bored with a Slocombe and a 3mm hole bored 20mm down it.

See Picture 124.

Into this hole a length of M3 threaded rod was inserted, this does not connect at either end and simply acts as a floating support and centres the two props to each other. There is a spacer nut which is CA'ed to the thread to prevent contact between the prop blades. The other prop was bored out to 6mm and a M6 threaded bar inserted into it and then CA'ed solid in the hole. The end of the hole then had a 3mm ball race fitted for the 3mm threaded end from the other prop to slide into.

See Picture 125.
See Picture 126.
See Picture 127.

THIS version of the torque convertor is going to be made with 6mm thick polycarbonate. It is thick enough for bullet proof glass -so I have hopes..... After the usual nasties of trying to saw polycarb -i.e. keep the saw cold and play a stream of water on it to make sure it doesn't think about getting warm. Polycarb melts at around 80C which is easy to produce when sawing and drilling it -sometimes the only way to extract your drill or saw blade is smash apart the thing you are trying make with a hammer and start again...

After due dictionaries of "words" and "pleas" I got my pieces cut and rough CA'ed then together.

See Picture 128.

The next step was the drill, (carefully), the re-enforcement holes and then tap them for the M3 bolts that would hold the sides whilst more treatment was administered to the casing... Tapping Polycarb is WORSE than tapping Copper. You forever live with the perpetual fear that what you are tapping into will melt and entomb your tap in it!!! I cut it 3mm at a time and "rested" the tapping Tee tool on a bock of ice. I may have suffered third degree frostbite -but it never stuck in any of the holes.

See Picture 129.

After having poured the best part of a bottle of thin CA around all the joints on the inside to both seal and strengthen it, I left it outside overnight to cure and it was ready for rough treatment to come...

See Picture 130.

As you can see none of the sides is the same height -despite my best efforts with a saw(!) I needed to produce a parallel face to the open face -this meant putting it in the milling machine. It is said that there are "Lathers" and "Millers" I am definitely a "Lather" as me and the Mill do not get on at all!!!!

After some improvisation in the clamping dept, it may look wild, but nothing would move -which was the point.

See Picture 131.

The edges were trimmed to height with an 8mm end mill and filled the shed with the evil polycarb snow that gets everywhere... A little further along and the casing now sports M3 tapped holes on the driven face and the driven prop has been test fitted to see it is clangs against anything when twirled -it didn't fortunately.

See Picture 132.

The final shots show the casing with the two props test fitted, (the driven prop clangs slightly and will have to be trimmed to diameter on the lathe).

See Picture 133.

See Picture 134.

The raw shafts will sit in ball races and have to have thrust bearing fitted to them. The next stage is the plumbing part and the problem of sealing the front plate. I do have gasket paper but I think something a little more robust might be needed(?) I keep looking at the pink silicone rubber pastry rolling mat but it might be a step too far in the domestic scavenging dept...

A summer evening has been spent playing with water.... I connected up the Torque Convertor and plumbed in the pump -which fed from a large jug of water. The Torque convertor leaked all over and to be honest I expected it to. BUT on the plus side it leaked very little from the face plate and mostly from the bearing holes.

See Picture 134.


The driven side is turned by the wheel brace clamped onto the shaft and the system turns quite nicely thank you!

See Picture 135.
See Picture 136.

I did some "Classical Physics" experiments with the the T/C as it was being pumped. To one side I affixed a 1 pound kitchen weight and then to the other side a 1 ounce one. Both  weights were connected to their pulleys via lengths of "button thread" and the 1 pound weight dropped over the side of the sink onto the floor. The 1 ounce weight rose a few inches in the time that the weight fell to Earth. Thus I can say that for every pound I put into the T/C I get 1/16th out. This multiplied by the gearbox gives me 90 ounces for every pound that I put into the T/C. I think the loco will move...

This raised the question -exactly HOW much force do I have to put into the gearbox to get the loco to move? After some due experiments with weights and thread I can state that the gearbox will move under 2 ounces of weight and the loco will move under 4 ounces of weight. Translating this into "real world" figures that I can think with...

The pulley wheel is 2.5cm diameter thus 1.25cm radius.
The force on it is 4 ounces = 133 Grammes
Thus the torsional force is 133 / 1.25 Grames per Centimetre = 106 Grammes per Centimetre = 1.08 Newton Metres

Which is not a lot and it shows how well the ball races are working.

Working back through the maths the loco will produce 1.08 / 5.8 * 90 = 16.76 Newton Metres

I think this loco will pull a couple of carriages...

The next step will be to produce a cylindrical shape inside the T/C as at the moment it is simply square. (I suspect that Joule was right on the money here and there is a lot of rotational enegy loss due to turbulence...) There being an extreme dearth of correctly sized tubes available in the house (i.e. none) I am going to have to cheat... There are two ways to do this; EITHER I take a short length of drainpipe and saw it into four quarters and stick them on the inside corners to produce a "cylinder like" shape for the water to move around in. OR I cut some sheet brass and roll a tube from it. The first option is by far the easiest and the second will produce the most accurate shape. Which ever option I choose the corners will require "packing" with P40 glass fibre putty to hold them in place and to stop the corners being distorted by the force of the water on them.

After having "sat down with a cup of tea" I am going to use the first option as it is by far the simplest.

The next thing I have to do is to "calibrate" my new T/C. The only thing that I have that I can say with decimal point accuracy in the rotation dept is the lathe. I do have an 80mm chuck that I can bolt onto it, (or the far heavier 100mm chuck), to provide me with a flywheel rotation at any speed from 100 RPM to 2,000RPM. All that is needed is a large rubber band(!) Delving into my collection of bits draw unearths an old belt from my turntable, it is a genuine brown fuzzy felt covered Dunlop SystemDek 3 that I have had since 1982 -and I wouldn't swap it for anything. It has undergone a few mods since I have had it such as; The Origin Live mods to the RB300 Arm, The Origin Live DC motor, The Goldring Elite cartridge (I used to have a Coral MC82 -unfortunately it just simply wore out....) The replacement vinyl platter mat for the felt one and the matching record clamp. This has added about 2Kg to the mass of the platter and makes it just dreamy to listen to!!! The only problem I have with it is the brown nextel suede is wearing off and it looks more than slightly bald in places (a bit like me!)

Anyway -back to the the T/C.

I know the rotation of the chuck to a decimal point per minute -thus giving me a linear speed for the 80mm chuck.
I know the diameter of the pulley (25mm) and thus the multiplication factor = Pi x 80/25 = 10.05

So it should be an easy task to ramp up the T/C to the full 4,500 RPM, (450RPM from the lathe chuck), that the props are capable of, and hopefully nothing bursts!

Well I found a length of 60mm ABS pipe and split it into 4 quarters and then stuck the pieces into the corners of the the T/C. This gives me a roughly cylindrical shape to play with. The next stage is to pack the cavities behind them with P40 fibreglass putty. Once this whole lot has set solid it then goes into the lathe and I very gently try to produce a cylinder from it with the boring bar. I did spend some time this morning looking at my loco and the shell that is going to have to go over it. The idea is that I hinge one end (the one without the engine!) and once the engine is running the whole shell then flops forwards on its hinge and away we go...

I tried four times to get the shell to fit....

It seems that despite all the measuring the shell lips are "just that bit" tight. So it is going to be out with the sanding block to take off some of the edges on the sealing lips. Once on the shell fits like a glove -but unlike the glove I seem to have a 3 fingers, a thumb and big toe on my hand!!! This is because I tend to produce "exact fits", and once something moves -or has to move in an arc -it just catches. If I engage reverse gear and drop the shell absolutely vertically on the frame -it fits. What is going to have to be done is that the lips of the shell are going to have to be ground to take a hinged arc motion. (sigh).

The epoxy set and cured overnight and a slow slightly squeaky time was had spinning the T/C on the lathe with the boring bar "doing the business" on the inside of the unit. I smoothed out all the lumps and bumps and took a smidgen off of the sides too (oops!) The gasket paper did work and here you can see the sheet stuck to the face of the the T/C -I punched the holes for the allen bolts to go through later.

See Picture 137.

The modified T/C is now being tested with weights and thread -and so far it has been quite an improvement. I knew that I was loosing some power due to turbulence -but to be honest I did not think it would be that much! The first trial showed that the 1 pound weight was now capable of lifting a 2 ounce weight at speed and then a 4 ounce weight showed that it would be suspended at any height. This shows that the now cylindrical interior of the T/C has improved the torque to the ouput shaft between 100% and 400%.

I have worked out the amount of torque that I am getting out of my T/C -now I have to work out how much POWER I am getting out from it.

Converting everything to SI (!) shows that the driving weight 0.453Kg takes 2.3 seconds to fall 0.8m.
 
This gives me that the input power to the T/C is [0.453 x 9.81] x [0.8 / 2.3] = 1.54 Watts

The output power from the T/C is [0.056 x 9.81] x [0.8 /2.3] = 0.19 Watts

Therefore lost to heat is [1.54 - 0.19] = 1.35 Watts

Pumping rate is 1.2 litres per minute thus the volume of water per second is 20ml thus the water leaves the T/C raised in temperature by [1.35 / 20] = 0.06 degrees Kelvin. Which may not sound a lot but I do now have some idea of how much heat I have to get rid of through the T/C cooling system. The modified surface cooler made from the Pentium II heat sink plus its 40mm fan should be enough. The problem is the volume of water that I have to pump into the T/C to fill it and then pump out the T/C to drain it. Whilst this is happening the loco is still being propelled!!! I think I have a workable system using solenoids to hold on a parking brake which draws its power from the "drain" setting of the pump and the best place to engage the "parking brake" is I feel on the main pulley from the T/C.

I am starting to run out of internal space rapidly....

What would be nice is to have a air bleed to the T/C so that when it empties I only have to pump out that volume and when it fills the same thing happens. I have an idea from the infamous "automatic brake bleed valves" from late fathers Westminster... I should be able to fabricate something similar from a couple of springs and two viton rubber spheres(?) Once this is working I then need to do some timing experiments on just how long it takes the pump to fill and drain the system. A timer cobbled from a NE555 should be able to do the drain time thing and then (once empty) it could then allow you to trigger the fwd/rev gear change. The fwd/rev would have to be a flip flop of some kind, as there would be instances where you simply wanted the loco to stand still -but still be in fwd gear.

Right. What you see below is my "doodle" of what the system should do (I hope!)

See Picture 138.

I have ordered the bearings and relays from my suppliers and it is up to "Her Pinkness" to cut felt washers to pack the sealing glands that the input shaft and output shaft will have pass through. I have no idea how leak proof greased felt is -but I can devoutly hope that it is better than what I have got at the moment. Yes there is a reason why the experiments are being carried out on the drainer of the kitchen sink....

Having used a device called a "Rotary Evaporator" in my College days I do know that centrifugal force will cause the fluid to cling to the sides of the the T/C as it operates and the air will be forced to the centre -and thus not leak (too much). I actually wish I had a Rotary Evaporator nowadays, the main use of it during my college days was to produce what would now be called "Bio Diesel" from the used cooking oil from the chip shop by the College. The fryers wondered what I wanted it for -the other students wondered how I got such good milage. It had to stop when the HOF thought that we were distilling moonshine and he refused to believe that it was DERV that we were purifying!!!

I am still debating whether to use oil or water in the T/C. One of the problems I think I might have with oil is that the props will convert my oil to dirty whipped cream -this was a problem that bedevilled early expreriments with turbochargers... I have this horrible feeling that the only way to know -is to try it.

The bearing etc have arrived via post -and today was the day that was scheduled for my Retinopathy examination. So, most of the morning was spent in a dark room recovering from the Tropicamine drops they put in my eyes. It stings like hell, and for about 4 hours afterwards everything feels like you are looking into a search light... But after lunch things had returned to normal and I started work.  I bored out the shaft holes in the T/C to 10mm and inserted the roller races then came the thrust bearings each side of the hole and (finally) the grease that should seal everything (hopefully!) The rather slimy result is shown below.

See Picture 139.

The next stage is to hack the hole in the chassis work of the loco to fit the T/C. I have this feeling that I am going to have to take a hacksaw to my chassis rails....

At the end of a Sunday "in the shed" I have fitted T/C version 3.... (And if this doesn't work I give up and go and cry in a corner). To fit it I did have to saw through my chassis rails on my loco -this does mean that one end of it is now errrmmm suspended in mid air whilst I figure out how to re-enforce it. I do have some wood that will probably be epoxied in place. It is like its two predecessors a "sidewinder" installation -how much this will affect the balance of the loco I do not know. You can clearly see the sectioned chassis rail with the bottom of the T/C now level with it.

See Picture 140.


This shot shows the front of the T/C. The output shaft is held in place with an external ball race. The output from the T/C pump is shown as the input side is now below the level of the deck. Both of them are equi-radial from the centre and (hopefully) once the fluid is spinning will ingress and outgress smoothly without too much foaming…. Once the fluid has exited the T/C it should then flow into the surface cooler and then back to the holding tank.

See Picture 141.

Tomorrow evening will most likely be spent soldering the electrical switching system for the pump and solenoid for the the T/C. Last Saturday I bought a few metres of "hook up" wire to begin building the loom for the loco. It is now time to take apart the lash ups for the cooling system and start hard wiring everything in place. The next step after that is to begin "hard plumbing(?)" the pipework into the frame. The next series of tests on the loco will concentrate on the T/C -should it survive first filling.... There was a recent "Mythbusters" in which they used Sodium Bicarbonate to break open a Gaol door -the pressure was less than 5 pounds per square inch. I have no idea what the pressure will be inside the T/C once it is running. It is made of 6mm thick polycarbonate which from my experience will take a Grade 2 lab explosion (100 Newtons impact) -my safety glasses are made from 8mm thick polycarbonate!!!

The question is -how much pressure will 6mm polycarbonate take with 3mm thick stainless steel bolts through it?

My son has asked me what would happen if I pumped a non Newtonian liquid into  the T/C -such as custard. I have to admit that frankly I have no idea… The theory is fine as the custard will act as a solid and still be liquid enough to be pumped -but I think this is a non-starter. There are better uses for custard -like with crumbles and pies!!!!

I will do the initial experiments with water as I have said and then switch to oil.

The test control panel takes shape! It will sit above the gear box and the silencer will sit behind the raised section of ply. The breakout tags are fixed to the ply with M4 nuts and bolts and ye olde piece of Vero Board has the relays mounted on it. They are from left to right; the fwds relay (DPDT), the reverse relay (DPDT) , the Fill T/C relay (DPDT) and the Drain T/C relay (DPDT). The switches are; the gear lever (DPDT centre off), the T/C pump control (DPDT centre off) and the main power switch (DPDT).

See Picture 142.

How exactly I get the gearchange to function is at the moment a puzzle... What the motor has to do is on the face of it is very simple -turn clockwise and then turn anti clockwise. There could be a simpe cheat (and I like cheats!) that uses a pick up track split into three sections. The two small end sections have a blocking diode on them arranged so as to face each other. A travelling pickup runs along the pick up track and the motor draws its current from that. Once the pickup has travelled into the facing end section the current stops. Once the current is reversed however... The diode now passes current to the pick up and the motor moves into reverse. Hopefully the following doodle will give you the idea.



Well I have had a busy day in front of the soldering iron and my eyes ache from straining to see things at such short distances -even with the magnifying glass from the set of "Helping Hands" and my reading glasses. Anyway this is the progress that was made on the Friday evening. You can see that the power feed for the relays as started to work its way across the tag strip -the main Positive feed for the board is on the lower right hand side below the bolt.

See Picture 144.

This is the underside. On the extreme top right you see the fuse holder -this is normally the thing I wire FIRST... The main on/off switch is simply being used as a SPST -but by having a DPDT witch in there to start with I can tag other functions onto the same operation (if  need to). The same is true of the Gear Change switch -although all four outputs are wired in I only use it as a SPST . The pump switch is always going to be SPST as all it does is connect relays -I can extract other functions from this switch via the tag strip connections.

See Picture 145.

The next shot shows the status at lunchtime. The gear change Relay is wired in and so are both of the pump relays. The Gear relay is wired BLUE and YELLOW the pump relays are wired in GREEN and YELLOW. I know that I normally use Blue and Yellow for DC of variable polarity but this simple  colour change will (hopefully) stop any cross connections. The solenoid side of the "fill" relay and the gear select enable side of the "drain" relay are not wired in yet.

See Picture 146.

By tea time I am the proud owner of technicolour squid... YES I know the cables are far too long and I can easily shorten them -the reverse is not true!!! There are a few connections still to be made, such as the interlock for the gear change relay, but since this will be a static test for the forseeable future -I am not too fussed.

See Picture 147.

Well after another day at the front... I tested the newly built control panel and found that, (somewhere), I have a major short circuit -Hey Ho! So, in the spirit of "Oh What The Hell" I unshipped the T/C and began testing in earnest.
Some Lucar connectors and a length of twin later I can report that the fill & drain system works and that whilst under test the T/C did not explode -although the seals on the rotating parts will have to be rethought....

The pressure inside the T/C was only 1.3 BAR and whilst it worked the amount of fluid loss was on the order of 75ml per minute and the volume of the ATF fluid container is only 250ml.

This may not sound a lot but the jet of fluid was at least 4 metres high and quite painful when I tried to stem it with my thumb. The tests had to be stopped at 3-4 minute intervals to top up the fluid tank, (red coloured water). The bottom of the garden now looked like an explosion in ketchup factory. Possibly I think again on how I circuit the fluid -there was a drip collector system on certain locos to deal with just this problem. I have to ask myself would it be a good idea to have the T/C simply vent to air and dribble down into a holding sump and pump from that? (Hmmm....) On the face of it that is not a bad idea and I will investigate that further over the comming evenings. It would involve changing what the feed sequence is to the T/C and cooling the fluid before entry into the T/C -but on the other hand this does mean that I can have a finned sump which might be a better option for cooling(?)

I am going to have to replace the M3 cap heads with epoxied lengths of M3 threaded bar and then produce a squishy rubber gasket as the std gasket paper with sealant compound that you use on the the car would not seem to be up to the job. This will enable me to apply rather more torque to the nuts on the face of the T/C than I can do at the moment. If I apply too much I will simply end up with M3 sized holes as I completely strip the threads there in the Polycarbonate.

The grease felt seals at the shaft holes do not seem to be up to much "cop" either... Repacking them and tightening them has reduced the dribble to a weep. What did make the most difference was lowering the voltage to the feed pump from 12V to 6V -but the amount of fluid that is going to have to go through the T/C means that the higher voltage will be needed. The tests with the kitchen timer showed that it took 8 seconds to fill the T/C -this gives me some sort of idea of how long to run the pump in reverse to empty the T/C whilst still having fluid in the pipes. On the shopping list for the next dollop of pocket money is a simple NE555 timer kit.

All in All a good first test!!! THIS IS THE FIRST ONE THAT HAS NOT EXPLODED....

This morning was spent trying to find the "short" on my new home made control board. I actually found it quite rapidly. That's the problem... I unlimbered my much loved and ancient "Smiley" AVO selected "Diode & Continuity" and applied the probes. I got an instantly lit red neon "short" across any part of the wiring. This I was expecting and some delicate work with a soldering iron unsoldered three connections. Two minutes proved that the short was not on the coolant feed relay system. A further unsoldering removed the gear change system from the list. The last thing on the board was the T/C pump system and I was very puzzled at this... I poked at the terminals and got a red light... I switched over to resistence mode and all became clear.

I had ZERO ohms between N/O and N/C connections on BOTH relays.

I had in short (!) two duff brand new relays...

One failure I would accept, but two failures on two relays -in the same mode??? I am not buying this brand of relay again!!!!

I re-soldered the red leads on the board to the coolant and gear change systems and then tested them and (hoorah!) they worked as expected.

After a quick trip to the local MAPLINS I have two relays that I have replaced the duff ones with. The main problem is of course that the leads are too short to fit them properly so I can see Saturday Morning being spent -re-wiring the wiring... They "clunnng" quite nicely and the flood / drain system now behaves as expected. Tomorrow I am going to visit the local B&Q to find some silicone sealant to see if that is the cure for the errrm "slight leak" from the T/C. I will build a sump system for the T/C as I think that this is my only real option -so at the moment I am building a shopping list of bits for it.

The next step once I have got a working control board -is to build the gear change system and its interlocks. This will entail replicating the "hand tuned", (well it sounds a lot better than being chewed to the right shape with a rasp),  wooden reach rod with one possibly made from metal. The linear actuator, (GOD I could really get in trouble with Trades Description Act from here on in), moves the reach rod through the gap and the pin causes the ballista to move the bevel gears across the graft gears. Well I gave in with being squirted at by th the T/C and returned to the problems of wiring and changing the gears. The gear change system has sat on the side of the kitchen for a few weeks now and to be honest it is way past it being fitted!

So, Saturday afternoon I sat down with a set of needle files an slowly worked "the shape" into a length of deal which would be the reach rod for the gear change "ballista" pin to be forced to move against. I did try brass but it was far to unco-operative. In its simplest form -it is a wedge... However due to the requirements of moving and locking the pin the actual shape is a delicately flattened 'S with a hook at the end of it. And if it is not absolutely true -it BINDS. It took nearly two hours of "Ho Hum" fitting and getting the reach rod through the gap until at last it lifted the pin across and then latched into position "like a good un". Now that I had a smoothly contoured shape it was time to fit the gear change motor to the reach rod.

This sits at an angle to the reach rod. As the motor winds the saddle down the thread the angle between the pin on the saddle and the reach rod becomes less as the reach rod is wound into the slot of the "Ballista". This makes the reach rod move initially fairly slowly and then at the end of its movement quite rapidly to lock the pin into its new position. The reverse action uses the hook and to grab and trap the pin against the slide thus slowly forcing the bevel gears across the graft gear. The screw action of the linear actuator provides a rigid termination to the movement.

I know it sounds complex but it is actually very simple!!!

See Picture 148.

Some slightly painful experiments showed that the reach rod "in" position is now designated as REVERSE and the motor has BLUE as positive. The stall current on the motor is about 6 Amps and it changes gear in about 0.8 seconds. There were a few ouch moments from hot cables and the motor casing!!!

Now that I have a working gear change -despite the protests of the motor. I then test fitted my control panel It is shown here only supported by two of the bolts and it sits directly above the gearbox -so I have to build some form of protective cage for the gears.

Yes, the leads are too long, however this is easily fixed with the soldering iron -and the may not be that much too long once they have been threaded into the loom and thence to where they have to go.

See Picture 149.

It is actually quite a simple board -the duff relays required the entire pump drain system to be rebuilt (ugh!) and their replacements are a little large in comparison -but they function well and that is all that I require of them.

The rest of my weeks time is going to have to be finding some way of making a seal on the power shafts of the T/C. Greased felt does not seem to hold much above 1 BAR so I am going to try to greased leather and we will see what happens.

After having had a good thought about it and slept on it I have decided to go out and buy some commercial oil seals. Getting the correct sizes proved to be far easier than I thought and the only problem I have at the moment -is the fact that everyone is on holiday. Since the same is true of the supplier that I will have to use to get the finishing things for the T/C, I am not overly concerned. The only seals that will fit are (typically) far more expensive than the normal ones used in the car world. They are both 16mm diameter and I am not sure if I have a mill of that size -but I definately have a "spoon" bit of that size. The polycarbonate is 6mm thick and the seals are 7mm thick. This means that I can legally sandwich the seals between two sheets of polycarbonate -I will have to cut an inset into the side of the T/C and then construct a flange with an inset to sit over the seal and then (somehow) stick the flange to the side of the T/C. This as they say is going to be "fun"...

Polycarbonate is the least forgiving material I have ever worked with -so I will have to make sure that everything that I use is icy cold and wet. There is a good chance that I will get even more wetter than I would get testing the T/C seals that I have made... But on the plus side I do feel that I am on the homeward stretch with this loco. I have gone through -"OMG I have had enough of this thing!" and the "Whatever made me try this?" to the "Now I am getting really bored with it..." and finally into the "It might actually work?!?!?" frame of mind.

The last loco I built, (The Krokodil), I kept a track of all the expenditure that I did and showed that it was possible to build a 1 metre long Gauge '3' loco for under £200. This week I will pass the £500 barrier, this makes it the most expensive loco that I have ever built and I think that I will be another £200 before I see it running on the tracks...

Having sorted through my tubes of mills I do infact have a 16mm end mill -still I am ashamed to say in its sealed and oily cellophane wrapper... So it must be New Old Stock from 2008 when I bought the mill(?) I now have to figure out how to do a "line bore" on the T/C to produce the two 16mm wide and 2mm deep inset holes on the sides. The easiest method is (I think) to fit a length of 10mm rod to the chuck of the end stop head and align the hole with the chuck. I then swap out the 3 jaw on the lathe for the collet head, fit the 16mm collet and then gnaw the inset into the polycarbonate -there is no other word for it! The outer shells will be dead easy -but messy. I simply carve a piece of polycarbonate sheet to the right size , true it up on the lathe, and then bore the 6mm shaft hole and the 16mm inset hole.

Everyone in the family has been told "Tomorrow Daddy is in the Shed" so apart from having to do the usual meal times I will not be disturbed. It is going to be one of those operations where it will take 2 hours to do the set up and 20 seconds to do the cut. Murpheys Law states that the required 20 seconds will not be granted me!!!

Well "Shed Day" started at 8 am with a good breakfast inside me and a couple of mugs of  lethal coffee. When I went to Uni I was given a kilogramme of coffee by my mother and told not to use it all before I returned home in two weeks time -I didn't manage it... After having delved through my draws and boxes, (thank you IKEA!), I had all the parts infront of me to do the transformation of the lathe. I unshipped the 80mm 3 jaw and changed over to the 32mm collet chuck. Some mutterings later I had the collet chuck aligned in the face plate. I make "patch marks" on the chucks to allow me to align them easily, some people dot them with a centre punch  -I file V grooves. It is easier to feel for them when you cannot see the location holes... I have a mixture of 3 and 4 stud chucks to my name and if you align the patch marks then everything slides home, the next problem is getting my not too dainty fingers to the nuts at the back of the chuck(!)

The next shot shows the vertical slide has been fitted along with some very "custom" mounting studs to hold the work piece, (i.e. the T/C), in the correct axial plane. This was established by fitting a 10mm mill into the collet and then sliding the T/C over it and then bolting the T/C to the vertical slide -thus the position of the hole is perfect!!! As my late father used to say -"You have to live in some bad houses before you get a home" and yes POP this is definately "a bad house". The 10mm is then swapped out of the collet. This he says so very glibly... The entire sequence is: fit the bar to the chuck, fit the crowsfoot spanner to the teeth on the collet cap. SQUEEZE both together to undo the cap, slide the mill out of the collet. Now COMPLETELY unscrew the cap from the chuck and then using "the knack" pop out the collet and replace it with a 16mm one. Now reverse the sequence...

See Picture 150.

The whole thing is then wound towards the mill at rate of 1.25mm per revolution of the crank until it touchs and then "backed off" a turn. Once the lathe has spun up to speed (about 400RPM) the T/C is then pushed into the end mill and after about 5 seconds -we have a 16mm concentric stepped hole for the oil seal to sit in. Given that the oil seal is 7mm thick I opted to cut 4.3mm into the wall of the T/C and the rest into the sandwich plate. This shot shows the stepped hole into the side of the T/C.

See Picture 151.

A length of scrap polycarbonate gives me the two sandwich plates. I would apologise for the repeat custom stud mounting, but it works -so don't knock it!!! Here I bored throigh the polycarbonate into the balsawood backing piece with an 8mm mill and then swapped that over for a16mm one. The whole thing is then slid across on the saddle and the process repeated.

See Picture 152.

A saw cut later and I have two plates to play with. A length of M8 threaded bar and a couple of nuts gives me a shaft to spin the scrap on and within the time it takes to boil a cup of water I have two outer seal covers. I have to say that I HATE working with polcarbonate -the one thing that redeems it in my eyes is the beauty of the finished article. The smaller of the two fits at the driven rear end and the larger at the front.

See Picture 153.

Ok a little shopping spree later at the local MAPLIN store.. I now own five 1N1001 diodes for the gear change motor system and a little NE555 timer kit for the not unresonable sum of £7. Could I have sourced the parts and built the PCB myself for that? I doubt it. So I am happy -as is the exchequer!!! I am used the Vellemann kits and this is a kit from a Uni here in the Uk. It lacks the detailed instructions of the Vellemann kits -it seems to assume you know what you are doing...

See Picture 154.


So it looks like another Saturday Morning at the soldering iron.

Saturday Evening has proved that it was correct! I now have a working timer board set to 7 seconds, (or thereabouts). I had to swap over the switch for the gear change to the one for the fill drain system -not a great problem. The reason is that the switch I was using for the gear change was a DPDT centre off and I only needed a SPST centre off. The other pole on the newly installed fill drain switch will connect to "Trigger" on the timer board. The idea is this. The NC side of the power relay allows power to the pump then the NC side of the relay on the timer then chops it off. So that regardless of the direction of current, I only get 7 seconds of power to the pump.

See Picture 155.

Sunday is occupied by "other things" as is Monday  & Tuesday -so it looks like Wednesday will be the next time I will get to play....

Well having grabbed some "free time" whilst the children party in the orchard... I have been devoting some thinking time to the problem of the Radio Control of the loco. I need 4 channels to cope with the amount of fiddling that it requires. I am going to buy a new 2.4Ghz R/C system, (I already use one for the NER EE-1), from the same people who sold me that one -the laugh is it is the same device but at £20 is only 40% of the original price... I need two sets of R/C controlled relays that can be made to Latch. This is a requirement to prevent sore thumb problems. The normal R/C flight layout are two joysticks -the left hand one having a graduated north/south setting for the throttle. I plan to use the right hand joystick to control the actions of the Torque Convertor pumping system. Thus east/west will be fill/drain and north/south will be gear change fwd/rev. The joy of latching relays is that it takes TWO flicks of the joystick to flip the state of the circuit. Thus I flip the joystick (east) to fill the T/C and then flip it (east) again to stop the pump and engage the solenoid parking brake. Similarly the drain system (west) operates and stops via the timer -the west position is set to non-latching. The north/south option on the right hand joystick is latching thus locking the gear into either fwd or rev. What I do with the east/west option on the left hand joystick -I am not sure(?)

Today has been one of those days in which you look around for someone or something to MURDER.... I found out why I seemed to be blowing fuses all the time. The batch of 10 Amp fuses I had got from Maplins were a complete waste of time. I tested the fuses BEFORE I fitted them and found that I had 7 out of the 12 that were there -already "gone" before I fitted them. I have spent nearly two days in careful and fruitless circuit dissection trying to find the non-existant short.

I then sneezed and yanked the daughter board with timer circuit on it. Needless to say it hit the top of the main power capacitor and the copper cladding on the PCB is no more.

Deep Breath...

I packed everything away and went shopping in town for the bits to replace what I had just scrapped. I will now replace the fuse holder with a circuit breaker. Even if it trips it will reset once the circuit is dead -or it has cooled again. So I might get bored with the waiting but at least I will be safe(!) One problem I have found with the timer board is that the "trigger" is an on/off setting -so I will have to work out some method of producing this once the drain option has been selected. (Is this what I use the east/west option for?)

Well after a Saturday and Sunday in the shed I decided to try out my new improved Torque Convertor. I did a static pressure test up to 1 BAR and nothing leaked -I was amazed!!! I placed it into the loco and wound up the system to speed with an electric motor (after having removed the glow plug).

1,000 RPM holding pressure 1.4 BAR
2,000 RPM holding pressure 2.25 BAR -idle speed on engine
3,000 RPM holding pressure 3.7 BAR -Torque convertor lowest "connection" speed
4,000 RPM -the system failed at a new point!!!

There is no need to test beyond 4,500 RPM as this is the maximum RPM on the prop design(!)

The plumbing system made of flexible polypropylene piping burst and I was thoroughly sprayed with home made ATF.... I had decided that the leaks from the front plate of the T/C were due to a lack of "depth" of seal -so I CA'ed a wrapper made of strips of ABS sheet around the edges of the T/C and then wiped the gasket seal around the new lip I had created. Despite the fact that I had to use quite a few tissues and paint brush cleaner to repmove the sealant from the lip of the T/C (and me!) it seems to be a suitable solution

There is nothing new in that happening, but it does mean I am one step closer to the actual running of the loco. If I can sort the plumbing problem out over the next few days I will have a go with a live test from the engine at the weekend. Closer inspection of the ruptured pipe in the morning showed that it failed at a point where it had been stored in a "kinked" position i.e. the pipe had been folded back on itself. Thus I presume it failed at a point where it had been pre-stressed (?)

Well I didn't get to fire the Fell over the weekend -I had other things of a domestic nature to take care of (ugh!). But out of it I have the parts to produce my parking brake system. This consist of a couple of gear wheels -with the teeth lathed off and some ply CA'ed to them to act as frictive material. This is also secured by a couple of recessed 2.5mm bolts -so if the CA gives way it will still hold together on the bolts.... The solenoid sits alongside the output shaft from the T/C and will pull on a "fork" fitting to push the two pieces of ply together. The solenoid has a convenient pair of holes that I tapped to M3 -despite their unwillingness to do so. The fork fitting is perhaps one of my finest pieces of self invention cum scavenging! It is the modified spanner that came with the IKEA light fitting that was put up in the kitchen on Saturday afternoon. The solenoid has a spring from a large biro as the return mechanism, (would I lie to you???) The spanner will be hack sawed to length later.

See Picture 156.
See Picture 157.
See Picture 158.

The last shot shows the ATF tank to the right hand side. This and the Glycol coolant tank are going to have to be replaced in the "running" engine.This is because I bought the biggest tank that "Just Engines" sold for test puposes. Now that I know how much coolant fluid and (soon) how much ATF I will require I can buy smaller ones. People have asked me "Why Glycol?" It is inert and doesn't have one of the more embarrasing problems of water -it has a wide freezing to boiling point range and it actually has a higher specific heat capacity than water. The mixture that I use is a commercial one for liquid cooling CPU chips PC's. Ideally the stuff that I would like to have pumping around my coolant system would be a saturated solution of Sodium Nitrite which used to be used for storage heaters -but with the amount of aluminium and copper around I doubt that either of them would last long!

I have decided that Sunday afternoon will be the time  that I test the torque convertor with the engine running and the wind it up past the stall rev point into the solid phase point and then over the other stall rev point. This could be very dangerous(!) The amount of energy contained in the torque convertor is frightening -in some respects it is like an angry captive genie in well shaken bottle... Something that you need but dare not open!!!!

The figures are simply nasty;

At 1,000 RPM The centrifugal acceleration is 33.54 G and the centrifugal force is 42.11 Newtons.
At 2,000 RPM The centrifugal acceleration is 134.18 G and the centrifugal force is 168.44 Newtons.
At 3,000 RPM The centrifugal acceleration is 301.96 G and the centrifugal force is 378.99 Newtons.
At 4,000 RPM The centrifugal acceleration is 536.75 G and the centrifugal force is 673.76 Newtons.
At 4,500 RPM The centrifugal acceleration is 679.33 G and the centrifugal force is 852.73 Newtons.

By Sunday tea time I should know whether I have a runner or a wreck...

It is now Sunday tea time and I am proud to say -WE HAVE A RUNNER!!! OK -so it might not move much, (the drive chains being disconnected etc), but the engine did fire after some very dire threats and the torque convertor did not leak too much. A forum member had requested that I make a video of this titanic event and I had to admit to myself that I had never used YOU TUBE in my life... So I opened an account and readied my tripod and camera. Then it threw it down and I had to rest everything in the corridor between the sheds -Hollywood never had this problem. I did make a small video sequence using my Mac and iMovie and uploaded it (it was quite easy to do!) Anyway here is the sequence:

The first part shows the glycol coolant system running -essential to any fire up -note that the pump and piping throb and the fan flappers move in the draft from the fan. (They are actually important -as it is very hard to tell wether the fans are working when the engine fires...) The second part of the sequence shows the torque convertor flooding and draining (note the rising level of red liquid). The third part shows the engine "on song" with my finger and thumb very painfully holding the throttle at the point of solidus -when the torque convertor begins to turn. Too much throttle and everything vanishes into blurs and grease gets flung EVERYWHERE -too little and the thing just sits there and laughs at you. Getting it right plus holding the camera by hand was not achieved without dire words to all parties involved. The first time I nearly got it right and then the camera battery went flat...

See video sequence fellpic159.

Well after dire threats I managed to drill a suitable expansion hole in the torque convertor. The one problem that I expected was heat. And this I got in barrow loads. What I did not expect was HOT FOAM. The dissolved air in the fluid was basically beaten out of the fluid and the cutesy baby pink froth returned to the reservoir. I had expected some "whipped cream" effect -but to be honest not a complete bubble bath...

Since the foam is compressible, whilst the fluid is not, very little happened whilst it was "foaming at the mouth" so to speak. So, what I have done is to drill a port at 45 degrees from the front face and inserted a length of 4mm pipe to as close to the centre of axis of rotation as I can. Now, (hopefully), when the torque convertor fills and froths, all the froth will rise to the axial centre of the torque convertor, and thus be expelled by the rising fluid. This does mean that I will have to block off the drain from the torque convertor and thus force all the froth and fluid through the central port until I get "clean" fluid coming out of it. How this will be done during the test tomorrow afternoon will be via applying by hand a pair of surgical clamps on the tubes. I know how long it takes to completely fill the torque convertor cavity -so it should be possible to set a timer circuit alter a valve to change over from axial port to radial port after the cavity is filled.

More Work (sigh)...

The loco uses a marine engine -thus the blue liquid is a glycol water mix with "Fernox" corrosion and algae inhibitor. This is pumped from the reservoir tank to the lower part of the cylinder head and thence to the radiator (which is fan cooled). The radiator consists of a XP1700 CPU cooler with a polycarbonate plate bolted to it through which the coolant is passed via a thin film. Not unlike the surface radiator system that cooled the Supermarine Spitfire. The red liquid is automatic transmission fluid (home made) and this is pumped into the torque convertor to engage the gearbox and thus the amount of fluid in the torque convertor varies the rotational speed of the gearbox. The used ATF is then cooled via a modified Pentium 2 heat sink (as above) and returned to the reservoir tank. The pinky yellow liquid is a home made glow fuel and is 20% castor oil, 20% Nitromethane, and 60% Methanol. I will admit it is very messy and I will rebuild the engine to use petrol and spark ignition when I get around to track trials as it throws used castor oil all over the place whilst running.

The next step of the development will be to fine tune the rate of flow through the torque convertor and the fluidus to solidus aspect of the ATF. This involves hot and cold viscosity tests. The viscosity of the ATF is determined by dropping a ball bearing down a glass tube and timing between two marks 30cm apart at the set temperatures (293K and 333K). Too thick it will not pump. Too thin it will not act as a solid at rotational speeds. More canubra wax thickens it, more rape seed oil and aniline thins it , (stir gently over heat...) The result from the kitchen smells not unlike a strange mixture of "cherry" shoe polish and frying chips(?)

I have three batches of fluid ready for testing tomorrow. YES -The Goldilocks Principle...

One is as thick as I think I can pump it.
Two is a solid as can make it between the viscosity temperatures.
Three is a 50/50 blende of One and Two...

Well at the end of a massively bad afternoon -here are the results...

One -was too thick to pump -it may in fact have been this that broke the pump...
Two -was "neither here nor there" from the standard mix that I have been using. Maybe it "came on" faster than the normal stuff but is difficult to tell(?)
Three -was maybe better at pumping and it felt "softer" than Two as it came up to solidus.

So, I now need a new pump for the torque convertor -this is not unexpected as the poor thing has been sorely abused since its purchase!!! It is is of the twin gear type and well it is missing a few teeth -rather like me...

Right. E-Bay has sold me a new pump for £4 plus P+P. And after the weekend I should be back in business.

I have to return to my plumbing problem, now that it works all the silicone plastic piping has to be replaced with curved copper with solder fittings -rather than "wiring them tight". This is where things get to the level of "inspiration"!!! I will have to cut away part of the re-enforcing  sheet of plywood underneath the curve of the bonnet and, (more than likely), cut away part of the longitudinal spars that hold the bonnet shape. I am going to have to remove the torque convertor and mark out the positions of the return plumbing. Both end faces of the convertor housing will then have to be cut into and a 13mm hole bored into it. The problem is getting all this plumbing into the confined space. The return is going to have to go from the LHS of the front face to the RHS of the rear face. Thus the fluid will move across the faces of the prop blades in the reverse of what they would do. This sounds strange I know -but work it out. The fluid will move around the cavity in an orbital motion from the outside to the inside and everything moves at a steady state. Which is all well and good -but what happens when we wish to accelerate or deccelerate? The return allows a flow of fluid to move directly across the blades -thus they now act as propellors rather than turbines. Once the fluid is moving at the same rotational speed, the return passes no more fluid, and the system resumes steady state.

Assembling the return is going to "interesting"...

The parts that will be inserted into the cavity faces are going to hasve to be epoxied into them. The first bend and its two short sections of pipe will have to be silver soldered together. The top connecting pipe and its two bends will have to be silver soldered together. The two unions between all three parts will have to be soft soldered together. This is not going to be "fun" by any stretch of the imagination. I will have to somehow melt plumbing solder near polycarbonate and not get it to melt... The obvious ploy is the mother and father of all soldering irons -the clamp on plumbing type.

Sorry for the delay in getting back to you... But there have been some domestic developments that take priority!!! I am now in the middle of converting the shed thus I cannot get any work done on my loco. The shed is sealed tight and (hopefully) not too much concrete and brick dust will penetrate into it. I expect to have to clean and oil etc everything that is in there. BUT at the end of the process I should have a shed with a nice insulated pitched roof and a plumbed in RADIATOR inside to help keep me warm. You know when you are getting old when you want to work on your loco but the prospect of sitting in near zero temperatures while you do so -makes you head for the fire and throw some more coal on it!!!

So,  have been doing some armchair research and bought a couple fo books from "the deadliest catalogue in the world". This is the one from Camden Miniatures. It contains all the books you never knew you had to have.... Out of the current issue I have bought Hydraulic versus Electric  -which is a study of the development of diesel  traction in the UK. Chapter Four is devoted the Fell loco. It contains the ONLY picture I have ever seen of the Fell Gearbox in situ. The inverted Y shape of the gearbox is plainly visible. My gearbox is "sideways on" as for me this made it far more easier to see that everything was working correctly. The chapter on the "convertor wars" was very interesting from my viewpoint as it clearly shows what they were using as a transmission fluid -DIESEL FUEL OIL(?) There IS a logic to this as the amount of fluid you need would be parasitic to the weight of the loco and the diesel would burn better if pre-heated.

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To Be Continued.